It was Jeron and I on the evening of the 27th in the Diesel Shop. We spent some time on the CE 15, our EMD SW1 that has been our primary switcher for the museum. I started by watering the batteries, adding about 6 gallons of distilled water, and then putting them on the charger. When Jeron arrived, we went over all the things we wanted to work on while it is in the shop for a few weeks. There were two belts on the Aux Gen that had come off the pulleys, the front radiator shutters were very sticky, and several other small items. We also made a list of supplies that needed to be ordered for the upcoming work. After that, Jeron thoroughly cleaned the headlight reflectors and lenses and lubricated some moving parts in the throttle to make it easier to move. I started working on drilling out the broken bolts and tapping the holes on the ground lights for the CB&Q 504 and replaced the sockets that were bad.
On Saturday the 30th, Mike and Matt started attacking the belts on the Aux Gen, by loosening the 4 bolts securing the Aux Gen and lowering the 4 adjustment bolts to drop it to make clearance to move the belts over the pulleys, and raise it back into position with a little more tension, then put the belt guards back on. I changed the fuel filters and Mike changed the oil filters. Jeron started taking the front screen off the radiator shutters to work on freeing those up. A lot of cleaning, dry lubrication, and some bending of some steel solved that issue. They work very nicely now. Colton went through the Aux Gen and Main Gen checking brushes, wiping down everything, including thoroughly cleaning the brush holder insulators. Jeron and I lubricated the front fan pulleys and tensioned those belts. It is at its maximum travel, and the belts are getting very worn, so we'll probably change them at the next inspection. Laddie spent a lot of time sandblasting many parts for the 33C. All in all, it was a very productive day.
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...