Wednesday evening in the shop was Kyle M, Jeron G and myself. We continued on the inspection items on CE 15. Before Kyle and I arrived, Jeron continued working on all the hood latches, removing any one that had bend or stiff linkage, straightening them as needed, and cleaning and lubricating all of them with a dry graphite lubricant. It is amazing how well and easily these doors close and latch now. All three of did the engine inspection, with Kyle on the right side, me on the left side, and Jeron and the bar turning the engine. During this process, we check the pistons, rings, and liners, a whole bunch of things in the air box and crank case. With no issues found, we moved onto other things. Kyle sanded and primed the surfaces where the front radiator screen bolts to the carbody, and finished by bolting the screen back on. Jeron started pulling the flange lubricators off to see if those can be repaired and put back into service. He was finding some very worn parts and it should be interesting to see what we are able to do with them, more to come there in the future. I spent some time removing the water sight glass, cleaning it, and reinstalling it. Much easier to see the coolant level now. I also changed both main reservoir drain valves.
On Saturday, it was Mike B, Jeron G and myself. Sorry, no pictures from this day as I just didn't remember to take any. Mike checked and oiled the friction bearings, went through the fuel pump motor and cab heat motor, cleaned some light safety globes and bulbs, and cleaned the rear headlight lens and reflector. I oiled the radiator fan bearings and then we both put the panels back in place for the duct from the fans to the radiators. Jeron started working on the sand hoses and checking more with the flange lubricators. After I had returned from a meeting and after we all had a late lunch, I went through all of the traction motors and checked the motor support bearings. All of the latch handles on the top of the motors were stuck, at some future date those will have to come off and have the pins replaced to make them work properly again. The cab floor and subfloor were all vacuumed. There's just a handful of items that remain before this inspection, along with some other improvements, are completed. Until next time.
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...