Monday, November 19. 2012
Diesel department weekend update Posted by James Kolanowski
in Diesel Department at
22:37
Comment (1) Diesel department weekend updateSaturday was a short day due to the monthly board meeting. Afterwards, Dan, Rod and I switched track 104 to clear it so a few cars could be moved out of track 4 in Barn 10. This was done so the B&G department can store the Santa Fe sign in a safe place indoors. It will be stored there until such time as there is funding and a location to restore and display the sign properly. For Sunday, the morning started with Jim and myself helping out Will and Jen to finish the tear down of the Terror cars on the west wye. The bridge that allows people to walk between the baggage car side door and the box car door had to be disassembled and the modules stacked in the box car. Between the walls and the deck, they are pretty large pieces that take a few people to move. Once that was completed, me, Jim and Kyle moved to the days planned activity of moving the ComEd 15 (EMD SW1) over the electric car department pit on track 41 to work on the #1 gear box. Earlier in the year, CE 15 was taken out of service due to some derailment damage to the #1 gear box and a broken pin on the brake rigging. The brake rigging pin was replaced to allow the unit to make two passes for the Diesel Days Parade of Power back in July. The bottom of the gear box was bent and split open from a failed weld on a side sheet to the bottom. We were planning on removing it for repairs to be made, but found a way to do the job in place. We welded a large eye bolt to the center of the pan under where the gear was and used a bar and hydraulic jack to force and bend the bottom of the pan close to its original position and welded the seam that was cracked open. A few packs of gear lube was added and the loco was moved back to yard 2 to be prelubed and started. We then switched a few more cars around, using CE 15. The last four Terror cars on the west wye were put away on the turntable leads and there were three flat cars in yard 13 that were in the way of ballasting track 134, so they were moved to the yard 13 lead. The loco was put away and we retired to dinner at a reasonable time for once. I hope everyone has a Happy Thanksgiving! Monday, November 19. 2012Storage in BarnsMuch of the work at IRM involves moving stuff around and rearranging the equipment for better access or to do a scheduled restoration task. After all we bill ourselves as a MUSEUM IN MOTION. Here is a wonderful photo from Phil Stepek who noticed that cars inside Barn 10 were being moved around a bit. It gives a great opportunity to see this in good clear light and to appreciate a fact. Restoration was done about two DECADES ago. The lettering on this side of the car was done over FIFTEEN years ago and most of that time this car enjoyed indoor storage. Protection under roof can clearly be seen as THE ONLY WAY TO GO. It is NEEDED if we are to be serious about preserving railroad history. Please enjoy this pic of our 1928 Pacific Fruit Express refrigerator car, and consider a donation so we may place additional cars into the next project, BARN 14. Please donate to fund RISWFC, on line, or mailed to Illinois Railway Museum Box427 Union IL 60180 Sunday, November 18. 2012
Steam Department Update 11-17-2012 Posted by Nigel Bennett
in Steam Department at
11:27
Comments (2) Steam Department Update 11-17-2012This weekend was "more of the same" at the steam shop, which was good as that is exactly what we need at this stage to get 1630 back together. Also, looking back, it is just about a year ago that I started logging detail of activity in the steam shop. It makes an interesting trail of what we have achieved so far. The focus is now on preparing tubes for fitting and progress this week was good: · we broke the record by swaging and annealing 43 tubes in the day. This is well over half as many as we have processed in all previous days combined. The other positive development is that several people learned the technique during the day so that we now have a number of people who can carry out this process. Here we can see Eric and Mark heating a tube in preparation to swage. And a nice shot of the swager actually forming the end of the tube. The one set back was that the ends of the last tubes swaged were not as smooth as they need to be. This proves to be the result of "mushrooming" of the edges of the dies. We polished this off in the evening so should be ready to continue next week. However it probably means that we should not do so many tubes at one time. We suspect that the issue may be that, over time, heat transfers to the dies and that is probably what allowed the deformation. Looking at the picture above it is easy to see how this could happen !!. · We started on loading tubes into the boiler and made good progress. 39 tubes were placed. We started at the sides as these are the most awkward to fit. Thanks to Roger for the photographs as I was buried in the smoke box doing the unseen bits!!. Most of the tubes in the bottom section will simple be pushed thru their hole in the front tube sheet and guided into the matching hole in the rear tube sheet with the ferrule already in place in the rear tube sheet. The ones at the side are more tricky. Because of the steam pipes, the tube cannot be passed thru its hole in the front tube sheet except at an angle that prevents it being fully inserted. So, in this area, the tubes are inserted thru one of the large super heater flue holes then moved to their actual location with help from someone in the boiler. Once in place, they are pushed forward to allow the guy in the firebox to fit a ferrule and then finally slid back into position. The picture show the external part of the operation and not Eric (in the boiler) and me (in the firebox) struggling in the confined spaces !!. · The stack of tubes on the fireman's side, that looked so large last week, is now virtually gone but we have a good supply ready to cut to length. We brought another bale of 37 into the swaging area. Very satisfying, there is now only one more bale left in the boxcar so the end is in sight. An interesting statistic on the tubes we are fitting. No wonder the piles look so large, the total length of the small tubes in 1630's boiler is a bit more than 0.6 MILES. · Another substantial task is Jerry's work on cleaning up the swaged ends of the tubes. Each must be polished with a sanding wheel on the die grinder to remove the scale formed in swaging. Jerry has put in many hours of work during the week to ensure that the tubes that we swage one weekend are polished and ready to use the next. So progress continues and it is really good to see obvious re-assembly work taking shape after so much stripping. The target will be to load all the required tubes before we start to expand them into the tube sheets. Actually fitting the tubes into the boiler starts the time clock on the certification period so we do not want to do this before all is ready to push forward. In other areas, Bruce was working on the detail measurements for rebuilding the axle boxes on 428. Nigel |
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Comments
Tue, 06-02-2026 19:38
Always a treat when a new diesel comes to IRM! Only wish we'd get more diesel department news from week to week, I always wonder what's going on in [...]
Wed, 04-01-2026 09:01
Good job on the barn 15
Wed, 03-25-2026 18:21
Exciting to see a new barn going up! What's next, after the RAIL project is complete?
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.