Tuesday, December 29. 2015
Holiday lights, Holiday trains, ... Posted by Roger Kramer
in Passenger Car Department at
19:05
Comments (0) Holiday lights, Holiday trains, Holiday decorations
Here is a pictorial about the Holiday Train event. IRM had a very successful Holiday Train event this year using for the first time, a diesel powered three CNW bilevel consist. This two weekend event was under the leadership of Paul Cronin, Coach department curator. It was so successful that we are increasing it to three December weekends in 2016. More planning is needed but already we are looking for volunteers to help expand our campus decorations. Anyone who likes to put up a Christmas tree and decorate it with all the lights and ornaments is invited to talk to Paul. We have a great opportunity to make Irm a beautiful 2016 Christmas wonderland! The possibilities are boundless! HO! HO! HO!
Looking West towards barn 9 as the Holiday Train moves out of the yard and onto the main line with the children and Santa Claus An interior view with a young family enjoying the train underneath the Christmas tree. Henry, you did a great job setting up the train. Now if we only had a building to house all those model trains. The new trolley buses were operating on the loop bring our guests from the parking lot to the Holiday train. This worked out real well. This gave our customers another ride while providing a warm environment. Sunday, December 27. 2015Steam Update December 2015
Another year draws to a close and there is a lot of activity in the steam shop. I had expected the day after Christmas to be fairly quiet but there was a good turnout and work proceeded on many fronts.
On #1630 we are progressing along what is now the standard plan for the Winter with the normal annual inspection work, which is substantially boiler focused, running in parallel with “catch up” work to improve the overall mechanical condition of the locomotive.
Aside from some smaller items, the major focus this Winter is on the valves. It has been apparent for some time that there is wear in the valves leading to lower efficiency and leakage that can be demonstrated when the valves are set in specific positions with steam applied. As with most backlog work, the initial hope that we could get away with a quicker and simpler repair has proved sadly misplaced!. Guess we should not be too surprised. When doing the initial stripping we found some tags set behind the valve chest nuts that indicate when last stripped for overhaul – SLSF Springfield shops 1947!. You really have to question the quality of the work when we have to do it again after only 68 years!!.
The findings so far are a mixture of good and bad news.
In parallel with the valve work, a lot of other tasks have been progressed.
On the Shay, work proceeds steadily.
On #428
On shop services, the large compressor is now fully plumbed in. As soon as we can get the power connected to it we can test and adjust it ready for the state inspection. With luck this will be ready when we want to rivet the smokebox of the Shay.
So a lot of activity but a whole lot more to be done if we are to be ready for running at the start of the season. So, Happy New Year to all and watch this space!.
Nigel
Thursday, December 24. 2015
Diesel Shop update from 12/19 and 12/23 Posted by James Kolanowski
in Diesel Department at
14:32
Comments (3) Diesel Shop update from 12/19 and 12/23While the 504 and 1848 were still in the heated shop to keep them from freezing, Jeron and I decided to work on a few little things that have needed attention. On the 19th, Jeron removed, cleaned, and reassembled the automatic air drains on the main reservoirs, and along the way found out that one of them to have a small crack in the housing near the manual part of the valve. It will be replaced later this winter. He also tracked some some other small air leaks, repairing some and noting some others for future repairs. There was a copper pipe on the drain side of an auto drain that had a split to it, that was soldered shut and put it back in place. Meanwhile, I started working on the air brakes. An issue started to occur where the independent brake would not stay bailed off. The fix here was to replace the 26-F quick release valve and the control valve which had a slight leak to it. At the same time a couple of filters on the air system were replaced. There is one more issue where we are waiting for a valve to ship from PABCO. Last night we spent a couple hours at the shop doing a little more TLC work on 504 and 1848. On 504, the platform crosswalk lights never had the lenses put in from when the restoration was completed years ago. They were just blanked over for the painting. I used one of the old fogged lexan windows from the bilevels and cut out a couple squares with the sawzall for the front and rear. Screwed and sealed it with some clear silicone so water won't get into it, let it dry and screwed the plates, with lenses, back in right before leaving for the night. The radio had quit working earlier this year, but we never had the time to troubleshoot why. A little bit of looking this time found no voltage at the radio rack and nothing at the radio breaker. Traced the wires back further into the cabinet only to find a broken one near the knife switch. Placed a butt splice on that and the radio works again. Jeron replaced a bulb on the transmit indicator as well. On the 1848, Jeron rebuilt one of the rear sander magnet valves that was sticking and leaking a bit. There is still more to do on these after some rebuild kits are ordered. We also straitened out one of the rear break away stanchions for the crosswalk safety chains that was not exactly straight. Over the next couple weeks, some other items will be done on both units before they get moved out of the shop and other equipment comes in for work.
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Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...