Sunday, March 1. 2015
Steam Department Update February 2015 Posted by Nigel Bennett
in Steam Department at
16:54
Comments (2) Steam Department Update February 2015
Unfortunately not the update that I was hoping to be able to write 24 hours ago!.
The steam team has worked steadily thru a record cold February and made good progress, primarily on the Winter work on 1630. The work on the boiler was completed and the objective is to carry out an initial hydro test as soon as possible to ensure that nothing leaks on the backhead where it would be hidden by the refitting of the stoker and footplate. We really need some above freezing temperatures to safely run the heater that brings the water up to a suitable temperature for the pressure test. This has held us up for a week or so but the forecast suggests a “warm” day Tuesday so everything was planned. The tender was filled last weekend to allow the water to reach at least shop temperature. On Saturday the pipework was set up and a start made on filling the boiler.
Unfortunately this revealed that one stay seems to have broken during the process of clearing the tell-tale hole. A steady stream of water was apparent as we filled the boiler. With this stay plugged, we were able to fill the boiler and prove that this is the only stay in this condition. However, we now have a stay to replace. This was something that was not in the plan.
By end of day, Dennis had cut out the cab floor under the engineer’s area, the end of the stay in the firebox was ground flush and the stay cap had been removed. This proved rather reluctant and took a couple of attempts, otherwise we might have got the stay out. Anyway, we are now ready to remove it next week.
Replacing a flexible stay is something we did several times during the overhaul and can be done in a couple of weeks, provided we do not hit anything abnormal. However, it is additional work and means that the target of running Memorial weekend is now in some danger.
In parallel with the boiler work a lot of other work has progressed.
Dennis has put in many hours of work building up the yolk and other parts of the tender draw gear support mechanism. We should be receiving a rebuilt draw gear unit shortly and then the work can begin on making any modifications required to fit this under the tender.
A new pin has been machined for the front coupler pocket. The original was heavily worn. Once new bushes are machined and the support plate, that Dennis has rebuilt, is in place we should have a coupler that sits horizontal rather than sagging as it has in recent years!.
The air tanks are now refitted. This has been a big job as we have fitted new Teflon seals to the ball joints of the tanks. It sounds simple but replacing the very worn seals that have been there for many years can slightly alter the fit of the pipes. There is very little flexibility in large diameter steel pipes!. So in some cases we have had to cut and rethread the pipes to make the correct fit.
The new bush for the connecting rod is now complete and in place in the rod.
Dennis built up the brass on the securing disk. (My mistake. I said last month that the odd one came from a Mikado. Actually it is from a consolidation). Once that is machined we will have all the parts to reassemble the running gear.
However, the first steps at refitting suggest that, with the new bearing in place, clearance will be very tight and it may be necessary to remove and adjust the axle box shoes. Measurements that Jason has made indicate that the shoes are marginally thick and will need to be adjusted at some point. It may be that point is now!.
Work has been proceeding on the replacement of the gland packing on the air operated power reverser mechanism.
After a lot of effort the broken bolt in the smokebox front ring was successfully removed and a new one is in process of being fitted. John Heid joined us and was rapidly at work on this.
When the work on 1630 has relied more on welding and machining, people have been able to do some work in other areas.
Progress has accelerated on the Shay.
The big determinant of how quickly the Shay can be brought into service is whether we can clear the tell-tale holes on all stays behind the frames and motor brackets from inside the firebox. If all the tell-tales can be cleared to the required depth, we then need just to replace a number of stays in other areas that have been identified as bad and can then move quickly to re-tubing the boiler. If any stays need to be replaced behind the motor bracket, then we have a substantial project to remove and refit the motor in order to replace them.
Several people have been working on this as time permits but Phil is now working on the stays 3 days each week and making good progress. A lot of stays have been cleared so far. We all wait with bated breath to see if any prove beyond clearance in the critical areas. We should know within weeks now if we can avoid removing the motor.
Various work has been progressed to allow reassembly to move forward if the stay work is successful.
JD has been locating and preparing the various parts of the running boards.
Brian removed the equalizer air tank and cleaned it in preparation for hammer and hydro testing.
(Brian’s comment on this photograph was very fair!. “You could at least have taken a before shot to show just how much muck I had to remove”). Located under the cab floor, behind the engineer’s footstep this tank gets buried is everything thrown up by the wheels. Good job Brian!.
On 428
The riveting team, led by Stu, has put in several days on the cab. There are a LARGE number of small rivets to be placed but they are progressing and the number of temporary bolts showing on the cab is steadily reducing.
Once it is at temperature the rivet is struck on the anvil to dislodge any scale and then put into the hole.
The bucker holds the head of the rivet in position as Stu uses the air hammer to form the other end of the rivet inside the cab.
Although the basic method is the same, these are far smaller rivets than we had to use on 1630. Rather than fighting to ensure that the rivet is formed while still malleable, the risk with these is more that they can easily be over hammered and have unsightly deformed heads.
The process of Dennis building up with weld and Eric then machining to final dimensions has proceeded steadily thru the many components of the spring rigging. With this now largely complete, work has now started on machining the valve rods.
Mike returned this week after being out of state for some weeks and work restarted on the planer in preparation for the axle box work.
So March looks to be a busy and critical month. Wish us luck!. And if you fancy getting your hands dirty ………!!
Nigel
Friday, February 20. 2015
Early February woodshop activies Posted by Roger Kramer
in General Blog Entries at
12:03
Comments (12) Early February woodshop activies
This news from the woodshop has been provided to me by George "Buzz" Morisette. Many different projects are being work on in our shop facilities. We all are especially thankful that we have this fine HEATED area to work on these many projects. Lorne Tweed has just finished painting the underside of the motorman's platform for our Cleveland PCC Bill is painting wood siding for the "Pennsy" Cabin car. Many people call it a caboose but in Pennsylvania RR terms it was called a "Cabin." This project will start this coming year. If and when the snow and cold ever leaves. Dave, also part of Freight Car Team, is painting more siding for the Cabin. What a fine job! Victor is looking mighty proud because the stove has been finally cleaned of dirt and rust.Here is a upclose shot of the insignia that was found underneath the rust. No doubt about it. It's a Pennys stove! Victor was showing everyone this headlight! This will be the headlight for the CGW Russell plow and is completely restored and ready for installation. Many parts were donated, scrounged and repaired to make this one whole. Good job guys! This addition will return the plow to it as built look. We could have used the Russell a few weeks ago. Rich Witt spends a lot of time at this table. Not pictured but receiving a lot of attention is the fine work Jeff Brady and Norn Krental are doing on the ME 28! Here Buzz took a picture of Randy Hicks and Larry Stone working on the 3rd rail beams for their ongoing project, CA&E 36 Here Randy poses for this picture. Buzz decided to take his picture since Randy is the one, generally, taking the picture.Buzz has been working on a new project for the display cars. It will be a new display case to house and interpret our many railroad lanterns. These oak cabinet bases have just been glued and are in the glue press for drying. This project Buzz has been working at home installing new wire or the future installation into the dining room of the Ely. This will be the finishing touch for a three year restoration of the ceiling in the private car. Buzz has acquired from the UPRR an original decal that will be applied later this year to our UP Turbine #18. Lastly, here is a view of the Electroliner sitting in Barn 4 waiting to be spotted over the pit to begin the removal of damaged traction motors. Rod Turner is leading this very important project! The motors will be then sent to a contractor and rebuilt to our specifications and then reinstalled. No easy task! Did you ever wonder what becomes of your donations to the various projects? This is a prime example of money being used from your contributions to better these projects and others around our museum campus.
With income tax season here why not consider a donation of some of your refund to a project or two at the Illinois Railway Museum. You will be amazed how we can stretch a dollar!
Thanks to Buzz Morisette for photographing the pictures and the idea for the update.
Roger
Thursday, February 19. 2015Fundraising Via Internet Social MediaWe have received approval from the Museum Board to expand our fundraising efforts through the internet and social media via GoFundMe. Please take a moment to visit the link and help show that this a viable avenue to raise funds for this and future projects. Thank you for your time and consideration. http://www.gofundme.com/mlfvx4
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Comments
Wed, 04-01-2026 09:01
Good job on the barn 15
Wed, 03-25-2026 18:21
Exciting to see a new barn going up! What's next, after the RAIL project is complete?
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?