Tuesday, October 1. 2013Steam Department Update 09-28-13It seems very distant to be providing this update from the UK. For the input I must thank Collin and Jim. The immediate good news was that apparently we did not put Ethan and Evelina off. Both were back and hard at work on Saturday. On 1630: · Rick, Ed & Collin concentrated on lagging the back head. First, the pieces of sheet metal were fitted up against the firebox to determine where and how they fit together. After having accomplished that step it was determined that the firebox door should be added next as it serves as a template against which the insulation is cut. The previous week the fire door casting, weighing several hundred pounds, was lifted into the tank's coal bunker with the forklift. A team including Rick, Collin, and Eric dragged the door over to the stoker coal feed pipe and placed it so the mating flange to the backhead was horizontal. Rick then mixed up the special fire-resistant concrete and mudded the flange. This mud serves as the gasket between the fire door and the back head where traditional insulation would be consumed by the fire. This is a tricky operation as the concrete has to conform to the surface of the back head before setting up yet be solid enough that it does not fall out of the flange once the flange is vertical. On the initial attempt the mixture was not set up enough so the acetylene rig was brought over to heat up the flange and speed up the drying process. Then a paper was tied to the top of the flange to hold the concrete in place until the fire door casting could be bolted to the back head. Once in place and torqued down, Rick mudded the flange interface completing the seal against the back head. As a final step to the back head project, Rick & Collin determined the appropriate width of the insulation for the back head is 2". Since our insulation comes in 2 1/2" sheets, Rick ripped down the sheets, one at a time and then cut them down the center as well. So, when work resumes next week, the back head insulation work can proceed as all parts are now ready. On Sunday, Tom and Cameron worked on aligning the fire-hole door casting with the stoker riser so that the securing bolts can be fitted. · Work progressed steadily on the boiler insulation as well. Eric, Jerry, Ethan, Evelina, Brian and Jim continued lagging the boiler courses. Since Eric has led this project and we had several new volunteers Eric became known simply as "Crew Chief". In totality, the lagging blocks are in place on the first, second and much of the third courses with a significant portion of the infill mudding also accomplished in these areas. · Jim Opolony picked up, from the wood shop, the cab window frame that Collin put his shoulder through two weeks ago. Many thanks to Bob and the guys for their efforts in producing the beading. Ed worked on the frame, cleaning it up and preparing it for the installation of the glass. · Dennis worked on the sheet metal for the smokebox. A number of the pieces were cut to shape and checked against the old damaged sections to ensure a match. · Tom and Ralph worked on the throttle. · Mike and Brian continued work on the valves of the air compressor. In other areas: · Phil and several others worked on preparing the steam locomotives on steam row for movement. More heavy duty switching is in prospect!. · Stu and Jane worked on the planer and have now primed the main pillar So it sounds like another successful weekend.. Nigel Sunday, September 22. 2013
Steam Department Update 09-21-2013 Posted by Nigel Bennett
in Steam Department at
09:52
Comments (4) Steam Department Update 09-21-2013It was a very productive day in the steam shop and, for once, the progress is very obvious. Two new volunteers came to the shop for the first time, Ethan and Evelina. As it turned out, it was one of those days when there were a number of things going on in which they could be fully involved so they had busy days. Hope we did not put them off !. Just about all activity was on 1630: · Phil and Brian did a thorough check of the smokebox, firebox and tubes to remove all tools and other items left over from tube fitting and other completed activities. A lot of what we are doing now seals up areas that we have been working in for months ........... so we certainly do not want foreign objects sealed up in there!. · Ed worked on the cab lagging and located the connections needed to link in the pipe to the steam chest pressure gauge. This is important as it has to be connected and run thru the next section of sheet metal that has to be fitted. The large casting of the fire hole door was lifted into the tender ready for refitting. Rick, who is our expert with the fireclay, was not around this week so hopefully it can be fitted next week. Brian and Phil cleaned up the parts of the butterfly door ready for fitting once the casting is in place. Much of the sheet metal for the backhead was sorted and moved up into the tender. This keeps it separate from the boiler lagging and convenient to where it must be fitted. In doing this we found the paint on a couple of sections was in bad shape. So Jane took charge of these, wire brushed and primed them. · Jane and Evelina used the thread chaser on the hangers that support the air tanks under the walkways alongside the boiler. Another job to ensure that key parts are ready for immediate use when we come to final fitting. · Eric continued work on the boiler lagging. Jim and Ethan ran a production line to split and taper the blocks to the required shape and Evelina worked with Eric to fit the blocks around the first two courses of the barrel. This is a thoroughly dirty job as the lagging breaks up easily and generates a clinging white dust. However, they kept at it and, by end of day, had set the lagging blocks around both courses and applied steel banding to finally secure them into place.
In the evening, Jerry and I experimented with the lagging mud. This is another unpleasant material. It is a dusty large grained powder that must be mixed with water to produce a sticky sludge that has a reasonable tendency to stick to things (including you as well as the boiler!!). With this we were able to fill the gaps so, provided it stays in place as it dries, the first course is now ready for fitting the sheet metal. · And then there was the major event!. As noted last week, we had set up the staging and brought in the super heater elements for the first row. Everything was prepared in the morning to start fitting the super heater elements. All the ball ends of the elements and the sockets into which they fit were cleaned. The channels into which the bolt heads slide were checked and cleaned. All the nuts and bolts had been prepared some months ago. In the afternoon, under Tom's supervision, the fitting started. Each element is secured by a special bolt whose square head locates into a channel in the super heater header. The bolt passes thru a yoke around the two pipes of the element. A specially shaped washer, designed to allow the yoke to bear evenly on both pipes is fitted and a special deep nut used to secure the yoke and so drive the balls of each pipe tightly and evenly into their sockets. The ball joints at the end of each pipe must then be carefully checked for alignment with their sockets. The nut is then tightened, ensuring that the ball and socket remain accurately aligned. The tightening requires quite a bit of torque as the environment around this area is pretty brutal. In operation it is in the path of the fire gases!. A production line developed. Cameron and Brian became the experts on the actual alignment and fitting. Sliding the element into place is tricky as the bolt must be in place in the yoke and its head must slide along the channel as the element is pushed into place. So you have the combination of sliding a 17 foot element along the flue and the bolt head along a tightly fitting channel. Once in place, the balls are carefully aligned into their sockets and held there as the nut is tightened.
Here, Ethan, Jerry and Jim feed an element from the staging while Cameron and Brian locate it into its flue.
As it became clear that the process was going smoothly Ethan, Bob and I started fetching the elements for successive rows from the boxcar. The longer down pipe are very obvious as Brian treats the bolt of one of the last elements with the anti-seize compound. The change in the boxcar is remarkable. From being full of parts a few months ago, it is now substantially empty. So we took the opportunity to put some of the rods from #938 under cover for the winter. By around 5:30 it was all done. 27 elements had been fitted. (Although built with 28, one was removed and blocked off before 1630 came to IRM so she now has 27). The view of the smokebox is now very different and 1630 now has a complete super heater again (subject to pressure testing in a couple of weeks).
· During the week Tom had worked on machining the throttle. That needs final lapping but is hopefully nearing completion. Overall a good day. I will now be out of circulation a great deal in the next couple of months, with a trip to the UK for a couple of weeks leaving today and for 4 weeks to Australia in mid October. Blog updates may be a little erratic for few weeks. I will need to rely on messages from the guys on what is happening to provide updates in the next couple of weeks. Then hopefully someone else can take over for a while. So, in the next couple of weeks, I will be awaiting the Sunday progress update like everyone else!. Nigel Sunday, September 15. 2013
Steam Department Update 09-14-2013 Posted by Nigel Bennett
in Steam Department at
11:13
Comments (3) Steam Department Update 09-14-2013
Work progressed steadily around some rather remarkable events in the steam shop.
I arrived Friday evening, ahead of the Board meeting to paint the back head ready to fit the fire hole door, to find the middle of the shop being set up as a left luggage office for a scene in the Transformers movie. Pity that I had not brought my camera that evening !.
Around the strange activities, I managed to do the painting and Dennis worked late, once they had finished, to complete a critical piece of welding. A few members of the shop team were around for the filming and, by mid-morning on Saturday, all the cases and other props were efficiently removed and we were back to normal (or whatever passes for normal in the steam shop!.
The switching for the film continues to provide views of the steam collection is unusual places.
Sadly I was not around to see 2903, 2050 and 265 pulled out into the open. They were back in barn 9, albeit not permanently as there is still a coach behind them, when I arrived on Saturday. The feedback from those involved in the switching suggests that the problem child was not 2050, as we had expected, but 2903. Despite concerns about the condition of her springs, the big N&W articulated apparently handled the curves and switches relatively well. 2903 apparently demonstrated in several places that the curvature was a good deal tighter than her long rigid wheelbase was intended to negotiate.
Everything continues to focus on what is necessary to get 1630 to steam testing.
· Effort was concentrated on lagging the firebox in the cab. This seemingly mundane activity is now recognized as critical. Even to test assembly of the super heater elements and valve chambers we need the throttle lever and other controls in place and steam / water tight. Since these are fitted on top of the lagging, this needs to be in place proto!.
A concerted effort by Rick, Collin, Ed and Phil achieved what we hope is the worst part of the job. An arch made up of 5 pieces of sheet metal runs from the footplate either side of the firebox across the top of firebox around the turret.
The pieces must be wriggled around pipes and the turret, little blocks of insulation squeezed under the sheet and the sheet metal joined by threaded rods.
Once the arch is completed in this
way, it is tensioned by tightening threaded rods that attach it to the
footplate. The arch must be completed
first as it secures the sections that are
formed around the corners of the firebox and these in turn secure the flat
sections on the back head itself.
This
was a really nasty job involving squeezing bits of metal, insulation, threaded
rods and small nuts into awkward crevices from confined spaces beside the
firebox and thru the cab roof.
The
guys achieved it and, by end of day the arch is pretty much complete and ready
to tension.
The
only known casualty was one of the cab windows that suffered a break the shape
of Collin's butt and is now in the wood shop for re-glazing!!.
· Work progressed on the boiler lagging. Eric has been concentrating on this and is becoming good at stitching the tapered blocks of insulation to the supporting wires. The first ring is now largely complete. The blocks are in place. We now need to finally secure them with banding, fill some to the small holes with insulating mud and then the sheet metal can be placed.
Jerry put in a lot of time during the week to ensure that all the sheet metal that was found last weekend is now painted and ready to fit.
· Ralph set out into the field to deal with the Koehring crane, that is used to load coal. It is really difficult to get coal into the high sided tender of 1630 with anything other than this old machine. So the fact that it has been unused since 2010 and not in regular use since 2005 was "a concern". Much to everyone's (including Ralph's) surprise and relief, it responded nicely to a well charged battery and some fresh gasoline and, in a few hours, not only was the motor running but he was able to test the operation of the boom and grab.
·
Jason and Collin worked on tightening the last
of the tube ends after beading and prossering.
As ever, the last two or three are always the worst. We preheated the water in the milk car so
that we could move quickly to pressure testing as soon as the work was
done. The process required a number of
cycles of bringing the boiler up to operating pressure, identifying the
remaining small leaks, carefully dropping the pressure, working the leaks and
then repeating. However, by late
afternoon the critical point was reached. We determined that the seal was good
enough to go forward to steam testing. So
the long process of refitting tubes is at an end.
·
This, and the excellent members' day BBQ, energized
the team and a lot of changes were apparent in a couple of hours in the late
evening. The gearbox, that has been a
feature of the smokebox for more than a year, is now gone and the smokebox is
wide open again.
Scaffolding was brought in to the
shop to provide the staging from which to install the super heater
elements. Feeling we were "on a
roll" despite the gathering darkness, a small group of us took the B&G
forklift out to the boxcar and fetched the elements for the top row into the
shop and set them onto the staging. We
are ready for a whole new activity next week.
So continued steady progress toward the steam test.
Nigel
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Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...