Saturday, January 3. 2009First Track Report of '09
Tom and myself were out today and knocked out another section of brush cutting on the mainline. My original plan to volunteer in the Library fell apart so Tom and I ran out to Book Creek Bridge and finished cutting the entire length of the curve including the area at and around the bridge which was, to say the least, an interesting experience. With a few hours of light left we ran to the far west end and began cutting eastbound. In this area only one side needing cutting so while Tom ran the south side I kept the machine stable by counterbalancing the north side. We cut the entire main from Jefferson St to west switch Schmidt, the UP interchange, Schmidt Siding and one pass East switch Schmidt to the West Station Switch. One more good day with some trimming on the mainline at Schmidt and between East and West Station switches, everything west of the big tree will be done. (~MP 1.6) I'd say we're about 1/3 of the way finished with the line.
In amazement, nothing failed or went wrong today... A few sprits of ether and she fired up, no hydraulic failures and no harm to hidden objects in the grass... This really is a terrific machine to have on hand. We will continue to mow the line as much as possible. It's fair to say we'll have the entire line mowed before revenue trains begin in April. That's the goal anyway. Adam Robillard Sunday, November 30. 2008Weekend track report
Saturday was myself, Tom, Frank and Trackbolt (Frank's daughter). We split ourselves into two separate gangs for the day. Tom and I spent the full day out on the mainline cutting brush with the recently debugged Amtrak brush cutter while Frank and Emily did a bunch of smaller essential tasks. The day started out like most any other day. The cutter wouldn't start. Immediately thought it was a dead battery (now only 2 weeks old) so we attempted a jump but nothing. Turned out the 60A main breaker fuse was busticated so Frank made quick work getting the last two from Napa. With a new fuse she started right up given the 32deg temps. Ready to roll, Tom set the cutter on the rails at Central Ave and we rolled out to Karsten's crossing to continue where we last left off. Things went well for the first five minutes when a hydraulic line failed...Typical day. Thankfully we were not stuck on the mainline without a way back cause Frank was on the grounds and went through our stock of used hoses and ran the motorcar out to us with the correct hose! We were back up and running in 10 min flat. A new record I think! From then on out the cutter ran great and we finished the first "section" from Karsten's crossing to the big tree were the RoW runs next to a field and we don't need to cut the south side. Satisfied we ran the mower back to Karsten's crossing and started the other direction cutting through the curve. Low light came upon us far too quickly and we quit a few poles west of the crossing.
Frank and Emily not only saved the day (twice), but also replaced a heel block bolt on the East Station 1/2 switch and capped off the leaking line on the Model 50 Burro crane. I'm pretty sure the two of them had to travel to every hardware store in the county to find the correct fittings, but they did and until we can repair the cylinder we'll at least be left without a puddle of oil on the machine. Frank mentioned an issue with a wheel locking up on the Santa Fe truck. We'll need to send it to Dave D. in B&G to take a look at it. Today I was out primarily to prepare for the Santa trains running the next two weekends. I cleaned the pockets on the 50th Ave/ West wye switch as well as the East/ West wye switch near Central Ave. Both locks on the switches on a shot of lub/ de-icer as well. The 50Ave switch got a little TLC and the switch ties are now spaced evenly and no longer crooked. Quick work with a lining bar. The mainline from East Switch to Seeman Rd, including Johnson Siding, was inspected and thankfully nothing major, pull aparts, were found. Julie, there will be a copy of the inspection sheet in your mailbox Saturday. I noted that the flange ways in Karsten's crossing were badly fouled so I cleaned them out. I think I've seen more derailments due to frozen crossings than anything and those CTA cars aren't that heavy. I finished the day with a cleaning out the bed of the Santa Fe truck and cleaning a few smudge pots for service next weekend. We have two pallets of kerosene switch heaters in the material yard so I found enough caps, wicks and pieces to get 6 put together. I was able to get 5 lit and working but I'll need to get another wick for the 6th. I dug them in and tested them out on the East/ West wye switch just after dark. They will be cool to use for the next couple weekends. I'm gonna try to be festive and get the two electric switch lanterns lit on the East Wye/ Yd 4 switch and the East/ West Wye switch lit as well. What's cooler than that...don't answer. Next Sat I plan a quick inspection of the mainline and get the pots and lanterns running and deal with any snow we'll have. Sayin 6-8 inches tonight for Union. Adam Robillard Sunday, November 23. 2008Second 1/2 a Track Report 11/23Frank and I were out today, naturally Frank was out Way before me though. Good thing because he installed the new radio in the Amtrak brushcutter where the old Amtrak one was mounted. Everything is installed ready to go minus the power to the unit. Nice work for sure. I arrived after lunch with the intention of getting the wine car parts unloaded from the UP hopper from California... Nick asked nicely. Frank had gone over the Model 50 earlier topping off fluids and repairing a tranny leak he found coming off the main pump. seems a lock nut was loose and was leaking at high RPM's. gonna have to keep an eye on that one. Frank was today's crane operator and his luck doesn't seem to be improving when it comes to travel mode. He was able to get it to move one direction but not the other. He found that pivoting the boom one way or the other made it function which tells us the contacts on the swivel post are dirty or corroded... After a while it worked fine so Frank said he'll clean up the contacts and hope that solves the problem.We picked up the UP hopper on station 2 and dragged it over to the steam leads where we picked out the 2 complete freight car trucks, coupler, diesel loco foot boards and steam loco firebox from the car. The car by the way, still has half a load of 20 year old coal in it. Thanks to Jim W and Dan M for running the USA8537 for the day. After lifting the trucks from the car, Jim W pulled the car out and Frank lowered the truck to the ground where Nick was ready with the forklift to move the trucks to Yard 10. Everything went smoothly including the unloading of the 1800's steam locomotive firebox that came along. To wrap up the day Jim, Frank and I dug the EJ&E 529 caboose out from 100 track and put it in Yard 11 for us to use with the Burro crane. The heat does work and I imagine we'll use it this winter. All in all it was a good day. Adam Robillard |
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Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...