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Sunday, July 29. 2012
Steam Department Update 07-28-2012 Posted by Nigel Bennett
in Steam Department at
16:26
Comments (10) Steam Department Update 07-28-2012Another good week in which we were able to move a lot forward on 1630. Various tasks support the overall work plan. First we must finalize preparation for the inspection of the boiler shell. Not much remains to be done to enable this so the next focus is on the tasks that will enable us to make the boiler water tight again. For this, we are preparing all the flues and materials that we need to refit the tubes and also to complete the patching of the firebox. Finally, whenever possible, we work on ensuring that parts that can be fitted once the boiler is watertight and passes its first hydro test are cleaned and ready to be fitted quickly when required. · During the week Jeff and Jerry managed to complete the cleaning and hydro testing of the super heater elements. The conclusions were good. 24 passed the pressure test at 1000 psi with no issues and are back in the box car ready for refitting when the boiler is ready. 1 passed the pressure test but has some minor damage to the protective shield (a simple sheet metal construction that is wrapped around the element to protect the most exposed areas from erosion by cinders flying thru the flue) and only 2 failed. The last 2 will require the attention of the boiler welding specialist when he comes in to safe end the flues. · Phil and Collin cleaned up the front tube sheet in preparation for re-tubing. · Eric did a great job clearing the medium from around the firebox. This is important so that everything is clear and visible for the upcoming inspection. The blasting medium is deceptive stuff!. We knew that there was some still on top of the firebox. The initial comment in the morning was "don't think there's much there". Having used an air line to blow it off the firebox crown and the stays at the sides of the firebox so that it settled into the bottom of the firebox water legs, Eric sucked it out with long pipes on the vacuum cleaner. By end of day we have a clear view along the bottom of all the water legs .......... and probably 80 lbs of medium extracted !. · After a lot of adjustment to get the settings right the McCabe was used to bend a test sheet for the firebox patch. Past experience with the Shay has demonstrated the importance of proving exactly how the patch will be formed using an old piece of steel before we do it "for real" with an expensive piece of new boiler plate. Considerable progress was made. The McCabe was used to bend the sheet
........... and the radius formed proved to be an excellent match to the critical curve in the mud ring. Having been cut to the template, the piece is a pretty good fit to the firebox and can be used to make minor adjustments to the template for the final patch. The next step is to form the piece to fit the slope of the front tube sheet. · Ed and Jim identified and measured the pipe work to be replaced along the boiler and this can now be ordered. · Phil, Jeff and I started another job that looks like it will be a lot more "fun" than we had hoped!. A number of the bolts that project from the front ring of the smoke box to secure the smoke box door sheet are wasted and need to be replaced. In theory they can be driven out by hammering them back (towards the boiler). In practice the effect of 60+ years of heat and rust on bolts that were a tight push fit to begin with is "interesting". After 90 minutes of effort with a heating torch and air hammer we have one out. Only another 15 or so to go !!. · Bob Hunter has now finished the computations and supporting documentation for the form #4 submission. This is the engineering assessment of the boiler which confirms that, having regard both to original design and subsequent wear as now measured, it is suitable for the intended operating pressure. This is now ready for submission. Nigel Sunday, July 22. 2012
Steam Department Update 07-21-2012 Posted by Nigel Bennett
in Steam Department at
17:36
Comments (0) Steam Department Update 07-21-2012I guess we must be becoming more adapted to the heat. There is not much choice this summer !!. A lot was achieved in the steam shop this Saturday and we are now moving toward the key step of the FRA inspection of the interior of the boiler. We have a few more minor tasks to complete inside but are now close enough to schedule the appointment. This is critical to our ongoing schedule. If the inspector is satisfied with the boiler interior we will be able to progress to painting the interior and refitting tubes. If any additional work is required that impacts the timetable. A number of tasks were progressed on 1630 · Chris and George from Curtis Boiler Service came in to scope and quote for the specialized welding of the safe ends on the super heater flues. George has done this work on several of our other locomotives over many years. He will also do the work on the rear tube sheet. · Work progressed well on the super heater elements. After the initial shock last weekend, when the first one failed, we now have 9 that have proved sound at the full 1000 psi pressure, have been cleaned and prepped and are now back in the boxcar where they will stored ready for refitting. Another 9 are outside the shop to be cleaned and tested during the week and next weekend. That leaves 8 more to complete the total of 27. (How does 1630 have an odd number of elements?. Because decades ago one position on the header was damaged and plugged so at IRM she has always had one less super heater than she was built with.) The process of cleaning and testing the elements is quite complex so I have made some notes below. · Mike has recovered and was back at the shop. He is in process of grinding the mud ring to ensure a smooth fit for the patch. · Glenn finished the McCabe and we took the first steps toward getting comfortable with using it and setting up to produce a test sheet that we can use to prove we have the correct radius to accurately fit the mud ring before we bend the rather expensive boiler plate. It looks as if Ralph has some doubts about what that lever does ! Phil working to set the test sheet in the jaws of the flanger. This provides a good view of the way in which the McCabe operates. The sheet slides between the flat surface on which Phil is setting it and the clamping head above it. It projects back toward the machine and extends over the curved die (the dark grey curved surface that can be seen below the light grey clamping head) into the space below the press head. The press head is at about 25 degrees to the horizontal in this view but would be drawn up to the horizontal to allow the sheet to be pushed into place. With the sheet clamped, the press head is driven down by stages bending the sheet to the radius of the curved die. The machine is hugely powerful, well able to bend 3/4 inch steel plate, and has few "fail safes". Only care by the operator ensures that it does not apply the force incorrectly and severely damage the machine itself.
· Ed thoroughly brushed off the various small pipes that run along the boiler feeding the lubricators and accessories such as the bell. The object was to determine if they should be replaced and the conclusion was that we should do this. Based upon examples such as this it seems safer to replace the pipes now. None were actually leaking but the objective is wherever possible to aim for a long spell of incident free operation and these have the potential to be a real nuisance. Once the locomotive is complete, these will be buried under insulation and lagging sheets. If one failed then it would probably damage the insulation and a lot of sheet metal would need to be removed to get to it. In other areas: · Tom has machined the spring retainers for the Shay so we can get those welded into place on the bolster fitted next time Dennis is in the shop. · Stu and Bob continued the assembly of the planer. Jeff had arranged for the department's BrownHoist crane to run in the Diesel Days parade and here it is running thru the depot road.
and comes to rest in the depot to be described. It must be a long time since she has been out of the shop and barn area. Cleaning and testing super heater elements Each element has been located in a flue thru which pass heat and debris from the fire. So they are thoroughly covered in soot and rust that must be removed before it can be inspected and tested. What Phil is doing here can be referred to as cleaning but most of us who have done it see it rather more as transferring the dusty muck from the tube to the operator !! The test rig must then be fitted to the element. The element has balled ends that, in service, are a dry fit into balled sockets in the super heater header. These must be carefully cleaned with emery cloth to remove pitting. A thin rubberized fabric washer is fitted between the test rig and the ends of the element. If this survives the 1000 psi test pressure the balls are in reasonable shape to make a seal with the header when they are refitted. Once in place the element ready for testing looks something like this. (Actually in this view the element is ready for the final step, after successful testing, when air is blown back thru the tubing to ensure that it is thoroughly dry and ready for storage in the boxcar. For testing the water supply is connected to the right hand side to the test rig). The rig is then connected to our high tech water pump. Joking aside, this may be old but is a very effective and critical piece of equipment that can pressurize the elements to 1000 psi and the whole boiler to more than 200 psi when carrying out a hydro test.
The loan of this tank from B&G overcame a significant problem last weekend. The pump operated very unevenly and Tom recognized that the problem was that the pump exerted sufficient suction to close the valve on the well if it is directly connected, even thru 100 ft of hose. Provided with an unrestricted supply the pump builds pressure evenly.
The pressure is raised to 1000 psi and the pump valve closed. If the pressure holds we have success. The most common problem is that a leak develops around the ball joints necessitating more work with the emery cloth and/or refitting of the test rig. Once an element has passed the pressure test, high pressure air is blown back thru it to make sure it is free of water. The rings that hold it to the header are carefully cleaned and sprayed with WD-40 to protect them and the element is then ready to go back to storage with confidence that it ready to fit into the header, hopefully during this winter. Nigel Sunday, July 15. 2012
Steam Department Update 07-14-2012 Posted by Nigel Bennett
in Steam Department at
21:24
Comments (2) Steam Department Update 07-14-2012Despite the heat work progressed well in the steam shop this week. A number of important tasks on 1630 were moved forward: · During the week, Kevin has made good progress on needle chipping the mountings under the boiler in preparation for painting. · Jason worked with Bob Hunter on the form 4 submission which is now well under way. · Glenn and Richard (welcome Richard on his first day) reassembled the McCabe which we urgently need to produce the firebox patch. An extremely awkward set screw fitting was achieved and the piston refitted. Now we are close to being able to test the machine. · Phil and Bob continued tapering the super heater flues. A welding contractor is due in next Saturday and we should then be able to start building up the flues ready for refitting. · Dennis welded the marks on the front tube sheet that need to be filled ready for tube fitting and also repaired the crack in the smoke box. We can now finish the front tube sheet ready for the inspection. That was the good news !!. The bad news was that Dennis proved that he is too big to reach the rear tube sheet either from the firebox or from inside the boiler. (Despite all the jokes, it is not your gut but your rib cage that determines this. I can just barely fit between the arch tubes and usually bruise my ribs when I do so, Dennis is just that little bit bigger in the chest). Hopefully the contractor coming in next Saturday is smaller and can do the work on the rear tube sheet. · Collin, Sean and Jason removed flexible stay caps that we need to inspect and Jason refitted a number that we have already done. Here you can see the inside of a flexible stay after cleaning and inspection. The slot is in the ball head of the stay surrounded by the hex headed sleeve. The stay is a long threaded rod with the ball head at one end, When fitting a new stay it is inserted from the outside thru the sleeve and screwed into the inner firebox. So far we have not found any bad ones, which is good news as replacing these is a slow job. · The big new task started, which kept a lot of us busy, was the cleaning and testing of the super heater elements. There are 16 of these and each must be wire brushed clean, the ball ends that fit into the header thoroughly cleaned and polished and then hydro tested to 1000 psi. While it will be months before we are ready to fit these, we wanted to start early so that we can schedule any repairs if required. It was a good thing we did. The first one failed the pressure test and will need to be rebuilt. Two then passed and the fourth proved to have a good deal of corrosion on one of the ball ends which will require significant work to reshape or replace. This shows the critical ball end of an element. The two rounded ends fit into rounded recesses in the header. It is essential that these provide a smooth, polished and rounded surface that mates tightly to the header. · We also welcomed a number of groups of visitors to the shop. It was encouraging that a couple of groups expressed surprise at the number of volunteers and amount of work being progressed. In other areas: · Jeff put together an outline plan for positioning machines in the new machine shop. Once this is agreed we will be able to position all the large equipment and free up a good deal of space in other parts of the shop. · Bob cut the steel slugs that Tom will now machine to make the spring retainers for the Shay and also continued work on the planer. Nigel Sunday, July 8. 2012
Steam Department Update 07-07-2012 Posted by Nigel Bennett
in Steam Department at
11:26
Comments (2) Steam Department Update 07-07-2012Another day with temperatures reaching 100 degrees certainly slowed work in the shop. However, we plugged along with frequent "cooling breaks" and made good progress on the key tasks. Alex and I completed tapering the safe ends for the super heater flues. So we are now ready for the welder to attach these to the flues. Paul cleaned up the pressure testing rig, that we need to test the flues once they have been welded. As shown below it consists of blanking plates that are tightened from each end of a rod so that will tightly seal the ends of the flue. One has the connections to allow water to be pumped in and air allowed out. Once free of air, the flue is pressurized to ensure that the welds attaching the safe ends withstand boiler pressure. Glenn, Phil and Jeff spent the day refitting the piston rod to the McCabe flanger. The rod is now in place. This view gives some idea of the power of this machine. The main cylinder shown here is approximately 3 feet in diameter. Operating at 90 psi this creates a force of more than 40 tons on a few square inches of plate in the jaws. In this way it can smoothly bend 3/4 inch steel plate with no apparent effort. The downside is that minor errors in adjustment or operation can cause this force to fall onto the machine itself causing issues such as the broken piston rod. There is some tricky drilling to be done to place a set screw but once that is done, we can hope to refit the piston and get the machine back into operation to start work on the firebox patch. Kevin has been working most of the week on preparing and then priming the tender tank top. This is a massive improvement. Unfortunately I failed to take a "before" picture but this area was in really bad condition, probably due to water lying on the tank top at some stage. Stu and Bob worked on reassembling the planer. A new bearing has arrived and the shaft has been machined so it is beginning to come together. Nigel Tuesday, July 3. 2012Steam Department Benefit at Sanfilippo EstateI have received a few notes from Jeff Calendine on the Benefit last Sunday at the Sanfilippo estate. First of all a big thank you to all who attended and made it the great success that it was. At this stage it looks as if we will have raised over $10,000 to support the ongoing work of the Steam department. I think it is true to say that a great time was had by all ..... I certainly I did!!. A huge thank you to Jasper Sanfilippo and the Sanfilippo Foundation who made us very welcome and allowed us to enjoy the superb collection of beautifully restored antique musical and other machinery. Here Jeff and Dave sit with Jasper with the Grant locomotive in the background. The steam engine house provides an example of the scale of the collection and the superb quality of the restoration A central part of the collection is the Super Wurlitzer organ on which Dave gave a masterful performance. In the carousel house, aside from the most spectacular 19th century carousel I have ever seen, is a collection of fantastic fairground organs. Here Nancy stands with Jasper in front of the spectacular 1906 Gavioli which replicates a 50 piece orchestra. Much to our enjoyment the carousel was operated for our visitors and here Dave and Jeff are seen riding on it. Many thanks to Jeff's brother Dave for a superb performance on the grand organ and to Jeff for the effort that he has put into the development and organization of this event. Plans are already in hand for an even more spectacular event at Sanfilippo next year so watch for the announcement of the date. Nigel Sunday, July 1. 2012Steam Department Update 6-30-2012Independence Day weekend and temperatures of over 90 degrees reduced us to a very small crew. However we achieved good progress on critical tasks. Working with Alex, we managed to cut all the safe ends for the super heater flues. The ends are laid out on the Shay bolster. All are matched to a specific flue. All 16 flues must have a small diameter safe end (the darker tube in the picture). 9 require safe ending at the larger end (the gray tube). The small diameter safe ends for these 9 are inside the large tubes. Each end must be tapered to fit into the end of the flue to which it is welded. This is a safety measure so that, should the weld fracture, the flue could not completely separate and fall within the boiler due to this overlap. The tapers are cut in the lathe. Here one is being set up for tapering With training from Tom, I cut the taper on a significant number of them during the evening. Tom can now arrange a time for the contract welder to come in and attach the ends to the flues. We also located the pressure test rig that we will need to test each of the flues after welding. Tom has completed the new piston rod for the McCabe flanger so next week we should be able to reassemble this in preparation for forming the firebox patch. It now looks very nice but provides a great example of the difficulty of working with old heavy equipment. Any breakage requires remaking parts in much the same way as repairing the locomotive itself. This apparently simple breakage has cost about $300 for steel and many hours of time in machining to reach this stage. We mentioned a couple of weeks back that the headlight had been refitted to 938. She now looks a lot better with the headlight in place. Now that would be a really nice locomotive to see in operation. Anyone got the odd couple of million spare ........... !! Hope to see many of you at the Benefit this afternoon. Nigel |
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Comments
Thu, 05-16-2013 21:52
Looking good Bob! I hope to come out soon once I'm done with school.
Wed, 05-15-2013 21:28
I was not around at the time. General discussion suggests that it was "pretty marginal" in a number of areas. Nigel
Mon, 05-13-2013 11:08
"THUMBS UP!"
Fri, 05-10-2013 02:15
No, it will not be necessary to hold any of the work waiting for the plow to be turned, end for end. Weather will be the major factor, but there will [...]
Thu, 05-09-2013 19:54
The CGW X-38 plow is really coming to life. Bob Kutella and Vic and crew need to be very proud of your collective efforts. I am very appreciative of [...]
Thu, 05-09-2013 15:20
The snowplow looks great! Are you going to apply the door and upper windows befor it is turned to continue work?
Thu, 05-09-2013 09:09
Max, Is there any progress to report yet, in regards to the installation of the poles and overhead wires? Have a good day, sir.
Wed, 05-08-2013 18:40
Thanks for the update! I still don't understand why Commonwealth #5 was removed from service. Do you know why?
Tue, 05-07-2013 09:28
Mr. Kolanowski.....I was just wondering if the Spaulding webcam will be up and running soon for us stay-at-homes. Thanks!2FP
Mon, 05-06-2013 23:04
Max, Has work begun yet on the construction phase of erecting the poles and putting up the wire? Wish I could be there to watch it happen.
Mon, 05-06-2013 23:02
Keep up the good work, Bob. Wish I could be there to help!!!!!!!
Sun, 05-05-2013 18:53
Ah yes, I have made such Jibs myself. If it were me, I would add in each corner an angled piece from the base to the Jib to act as sway bracing. [...]