Earlier in the week on Monday morning, Dave Diamond drove the wheelset that was removed from 6847 along with the new motor to a shop just outside of Chicago. They pressed off the wheels and gear, machined the bearing surfaces on the axle, and pressed the gear and wheels back onto the axle and reassembled the combo with new support bearings. Initially there was over .350" of lateral between the old motor and wheels, which is out of tolerance. After the machining and pressing the gear into the correct place and after reassembly with the new motor and bearings, the lateral was .079" where it should be. Dave Diamond helped us out again and picked up the combo on Wednesday morning and unloaded it in the steam shop under the overhead crane.
Saturday morning, Roger Broms, Dan Currens and myself arrived and started to do some other prep work including replacing a broken bolt on the nose pack, and then compressing it to be reinstalled once the motor is back in the truck. The nose pack is basically a rubber pad sandwiched between two thick bars of steel, which supports the nose end of the motor against the truck frame. We also mounted the blower duct and roller bearing boxes and then moved the motor to the drop table.
The Steam Department volunteers helped us out again as well by getting the drop table ready to go and helping get some tools and supplies, as well as operating the crane to stage the combo on the drop table for the installation. The 8537 was used to push the 6847 onto the drop table, centering the #5 axle over the table. The position of the pedestals was marked on the table, and then the table was lowered a bit and moved to the west side of the pit. The centerline for the wheels were marked and then the combo was placed with the nose of the motor blocked up.
The table was lowered and moved back to the east side of the pit under the loco, and raised back up stopping occasionally to check clearances and to line up the roller boxes with the pedestals. We had to push the firemans side wheel over just a bit with a bottle jack to get it to line up exactly in the pedestals, then raised up some more. Eventually the motor nose supports lined up with those on the truck frame and we slid in the support pack and pinned it in, lowered a bit to remove the blocking under the motor, and then continued to raise the table until the springs seated properly over the roller boxes. The table was clamped back into place and the loco was moved back into the shop.
We then put the pedestal cross bars back on, remounted the brake shoes and shock absorbers, released the bolts holding tension on the rubber nose pack, hooked up the traction motor leads and inspected a few other items. After all that, we moved the loco back outside and Jim West helped move the 428 and Shay back into the steam shop.
There is a gallery setup with some random photos during the process of changing the combo, http://www.irm.org/gallery/diesel-november2010, they are mostly in order from the prep work, to removing the wheelset and old motor, to installing the new motor and wheelset. Thanks to everyone that helped during the entire process. Next year when the weather is warmer, we'll test everything out operationally and CNW 6847 will be back in service again.
We seem to be falling into a winter work pattern, with Saturday by far the busiest day in the shop areas inside Barn 4, then Wednesday, and Sunday holding onto third place. So take note that there is more space and less competition for machine time and bench space on the latter two days, if you want to work on your favorite project, or to just show up to watch and help the others.
Jeff Brady is working to glaze the top three openings on a new baggage door for Michigan Electric 28. This is a good cold weather project, when the barn space is really too cold to accomplish a lot. Ray Schmid is in the background painting the retainer beading for the glass.
Bill Moran was on hand and we decided to start the process of planing stock for a new roof on the Los Angeles coach using the planer to reduce the thickness of the new lumber (sawn on Saturday), to the planned 7/16". Here he is removing one of those 16 foot long strips from the outfeed end of the planer.
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]