Tuesday nights work on the Green Bay and Western 2407 was to fix more leaks on some of the water pipes. Jeron Glander, Dave Fullarton, and myself arrived about 6:30pm and spent about four hours working on it. We started in the cramped quarters of the radiator room, using the porto-power to move one of the main water pipes around, bending a mounting bracket straight again and getting 3 main points of the pipe to line up properly. After a lot of adjusting, the sleeve fit perfectly. Then Jeron and Dave wire wheeled the surfaces of the pipe where the rubber gaskets of the coupling will seal and then reassembled the coupling and tightened up all the clamps.
After that I removed a small 1/2 x 8 inch pipe that was cracked, removed the reducing bushing that had the broken portion of the pipe stuck in it, removed the broken portion and replaced with a new pipe. Naturally, it has to be in one of the worst spots to reach, between the oil cooler and main water pipe, blocked by the drive shaft and eddy current clutch and guards, but we were able to squeeze in there and get it done.
Dave did some vacuuming of some debris on the floor before he and Jeron moved on to the engine to start taking off some water elbows between the head and block. There are a number of gaskets on the engine and air compressor that are dried and split and just need to be replaced.
I have created a photo gallery of the mechanical work as it progresses. There are also a few photos of the cab and the fogged and bad windows that need to be replaced. These will all have to be replaced with FRA glazing, donations to the RSD15 would be greatly appreciated and will assist in the costs of the restoration.
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...