Sunday, October 7. 2012
Steam Department Update 10-06-2012 Posted by Nigel Bennett
in Steam Department at
12:16
Comments (2) Steam Department Update 10-06-2012A day of steady progress in the steam shop. The main focus was on refitting the tubes into 1630. At the moment it is all preparatory work to ensure that we can establish a "production line" process when we do the actual fitting. · The major step, with considerable assistance from Bob and Joel in the wood shop, was the production of a measuring beam. This is based upon Tom's experience from the last overhaul. The problem is that the distance between the front and rear tube sheets is about 17 feet and the sheets are not perfectly even. Each tube needs to have a fairly accurate 1/4 inch projection beyond the tube sheet each end and the variation between the shortest and longest, due to the variation is the sheets, is around 1/2 inch. So, to cut all to a standard length and grind down to the exact length would be a VERY slow process. Also test fitting each tube into the boiler in order to mark where to cut is very hard work. So, based upon Tom's experience the beam provides a much simpler approach. It was made with a hook at the rear end which, when passed thru the hole in the rear sheet, will hold the beam accurately to the face of that sheet. (Don't worry, this was taken before the hook was finally tighted onto the beam!) The other end is marked with colored bands at 1/8th inch spacing. We simply note which band is visible at the front tube sheet, mark the hole with that color, and repeat for 180 holes. We can then cut tubes to 4 lengths (1/2 inch longer than the measurement) and fit to the holes based upon the color codes. It will take some time to mark up the whole tube sheet but will save a great deal of time overall.
The other challenge that we confirmed in this exercise is a little anomaly with 1630. Normally the pattern of holes in the front and rear tube sheets is the same, which means that you can simply count vertically and horizontally to match where to place a tube. Snag !. Somewhere along the line, probably when the rear sheet was replaced in the late 1930's, 1630 acquired sheets that do not match front to back in some areas. This means that we have to be very careful in matching the holes when measuring and then number them at each so that we can place the tubes correctly later. It will be a LOT easier to make sure we have everything matched using a timber beam than to try and match using heavy steel tubes !. · Production of ferrules continued steadily. We produced about 40 so we should have the supply in hand by the time the length measurements are complete. The objective will be to place all the ferrules in the back sheet in a single exercise once we have done the measurements; · Glenn and Jerry cleaned up the ends of the tubes that we swaged last week. This points up a learning. The mill scale on the new tubes is a lot more difficult to remove once it has been heated and swaged. So, in future, we need to wire brush the new tubes before we swage. In other areas: · Work progressed on the set up of the "new" house air compressor. New is a relative term as it is an EMD locomotive compressor of 1950's build acquired from a Milwaukee Road shop. However it is an important pre-winter task as we will use a lot of air in tube fitting and riveting the patch. The existing compressor is getting "tired" and past experience is that digging the Sullair out of a snow drift and starting that up makes for a slow start to work on a winter morning. This is a major enhancement that is being funded from the annual Sanfilippo benefit. The compressor site has now been cleared and work is starting on set up. The site is subject to review. There are concerns that the compressor will be too noisy when running in the shop and it may be best to site it outside. However that could not be done until Spring to coordinate with B&G work on the shop. As very little change would be needed to piping or electrics between the two locations, we will set up inside now and decide, based upon experience over winter, if this is the permanent location. · Bob and Stu worked on the wiring for the water supply that we need to change to make it more readily usable next year. (It was a little embarrassing that the Leviathan team ended up using a fire truck to get water as the water system was so tricky to start). So a reasonable day of progress on several fronts. Nigel Sunday, October 7. 2012
CGW X 38 Update - October 6, 2012 Posted by Robert Kutella
in Chicago Great Western X 38 Russell Snow Plow at
09:25
Comment (1) CGW X 38 Update - October 6, 2012Saturday saw some work continuing on several smallish aspects of the restoration project and one much larger effort. The day started by taping up a sheet of mylar to the south side to trace and document some of the lettering. Who knows what future generations will want with this equipment? It is important to document and preserve its history at any stage. In the woodshop, Buzz Morisette volunteered to help me out with both of us fabricating several new pieces of millwork for the project, and Buzz prime painting some of them. This view shows the remaining stop jambs needed for the south door, and three pieces of drip caps that Buzz made for his work on Milwaukee Road equipment. We also made two small stop blocks for window framing and two large nailing timbers for the rear two inside corners of the plow. A big thank you to Fred Ash who spent virtually all day on the rear wall, on the business end of a needlechipper. Almost all of the remaining old paint is gone as we race the calendar to get this wall primed and finish painted. This project is an interesting study in volunteerism at IRM. In just four short months of summer work, a new crew has made remarkable progress in preserving and restoring this plow. They have developed new skills, a strong sense of ownership and pride in their work, and made new and lasting friendships. It shows what can be done with limited financial resources but with a willing and ample supply of volunteer labor. Wouldn't you like to part of such an effort? Come on out and join this TEAM, or if you rather, see me about putting together a few of your friends to start work on your favorite car in our collection. We have plenty to go around! And do not let the approaching cold weather stop you. We plan to work indoors throughout the winter fabricating new doors and windows for the plow, and there are several other varied and diverse projects waiting in line. Sunday, October 7. 2012Wood Shop Update - October 6, 2012There will only be a few short reports this time. In the areas I frequent there was not the typically large turnout of volunteers - maybe they were all out shopping for their Halloween costumes. But still a LOT of activity around the campus. If any of you would like to see more reports or more coverage, why not grab your digital camera and come out as a REPORTER? We could definitely use the help in this respect - in the areas I cover and for many of the other departments where work does not get reported and shared on a regular basis. Heavy lifting NOT REQUIRED! We were happy to welcome some members of the Steam Department into the wood shop, including the smiling Nigel Bennett, esteemed BLOG REPORTER for that department. They were making a sort of gauge stick, or story stick to assist with measuring each individual tube length for the FRISCO 1630 decapod. There are minor variations in the 'flatness' of the front and rear tubesheets and they hope to custom fit each tube to a particular opening. Eric Lorenz was working to replace bottom rubber gaskets on the over 50 windows needing it for our Cleveland Transit System 4223 PCC car. They are a very special cross section, found by Lorne Tweed and now on hand. Getting them into place is another story, but Eric has worked out a procedure for both the upper and lower windows. |
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Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]