Sunday, February 10. 2013
Steam Department Update 02-09-2013 Posted by Nigel Bennett
in Steam Department at
13:52
Comments (2) Steam Department Update 02-09-2013While it was a part day in the shop for me, as I attended the Board meeting in the morning on behalf of the department, a larger team braved the snow and ice and good progress was made in a number of areas. On 1630: · the first of the cladding sheets, as well as a number of cab fittings were brought down from storage above the machine shop for inspection, cleaning and painting. There is a great deal of this to be done in preparation for the time when we will be able to start refitting them. Much of this is an unpleasant, dirty job as the sheet metal must be wire brushed to get rid of rust and bits of lagging. However there is now an area set up to allow cladding sheets and other parts to be painted and allowed to dry (at the opposite end of the shop from the dust generated by the cleaning process!).
Above are some of the first results including sections of the cladding, that make up the covering of the boiler backhead in the cab, and the mounting plate for the pressure gauges. · on the tube fitting there was significant progress, more in the areas of developing processes for the next steps than in fitting large numbers of tubes. o While I was at the meeting, Collin and the guys completed removal of the rogue tube from last Saturday and put a new one in. o The new roller has arrived and we spent a good deal of time working out how best to use it. This roller is designed to both expand the end of the tube and simultaneously flare the projecting end of the tube, ready for beading. We used this to start work on the smokebox tube ends. The size of this roller should allow it to be used on both the firebox ends and those tubes at the smokebox end that require beading. Because it is a great deal easier to work in the smokebox we decided to work out how best to use it on smokebox tube ends. This proved to be a very good decision. It certainly does expand and flare the tube ends quickly and effectively. Once in place and properly driven, the process is complete in maybe 30 seconds. The snag that became obvious was that the additional force required to turn this roller, as it not only expands the tube but flares the ends at the same time, is more than our smaller air motor can provide. This is a significant issue. The smaller air motor weighs about 30 pounds and can be reasonably controlled by one person. The bigger one drives the expander with no problem but weigh 50 pounds or more. Manually supporting and locating this beast on to the expander for every hole, which we can easily do with the small motor, is pretty exhausting work for two people, as Phil and I found out. Some more development is required. While we certainly could expand the smokebox ends this way it would be slow. The operators require frequent breaks!!. Next week we will need to explore other options. We probably need to find ways of supporting the motor in places from which we can drive the expansion of multiple tubes using the flexible drive shaft, rather than attaching the motor directly to the expander and therefore carrying the full weight of the motor to every tube end. Clearly we need to develop methods that can also be used in the firebox. ... If the big motor is tough to handle in the smokebox it will be a nightmare in the firebox with the arch tubes in the way!. o Despite this we successfully expanded a number of smokebox ends. I have changed the progress measures to reflect the way we now expect to work. At the smokebox end only some tubes need to be flared (those that will subsequently be beaded) and we will do this simply by using a different roller for the expansion. So this weekend we actually flared 7 and left 4 un-flared as they will not be beaded. However in all cases this did all that we need to do to the tube before the first hydro test. At the firebox end, flaring will be a separate step. Beading will not be done at either end until after the first hydro test (so that any leakage can be corrected by additional rolling). Here you can see the results on the tubes directly below the super heater flues from column P and to the right where the ends are now flared when compared to the raw tube ends in the rows below. o At the firebox end we continued to fully seal tubes that were previously set into place. Unfortunately we still hit an occasional one that shoots out the ferrule in this process and needs to be replaced. This seems to happen with those tubes that were originally set with the roller rather than they expander. At least we are now largely thru the ones that were set in this way. · The sight feed lubricator was located and Jerry started work on cleaning and checking this essential component. · The ring spacer required for the one super heater flues with an extra large hole was completed ready for refitting of the super heater flues. In other areas: · Jerry and Mike made good progress on clearing the shelving at the South West corner of the shop to make an area against the wall to store the McCabe flanger. This will be a major improvement. The flanger is, on occasions, a critical machine and had a major role in producing the patch. However, between those occasions, it a huge lump of metal that cannot readily be moved any great distance and takes up a lot of useful space!!. So the objective is to provide a storage space against the wall to free up useful space in the fabrication area when it is not required. It would be really nice if we could store it out of the shop in a container. However, it is so heavy that only the large Buildings and Grounds forklift can handle it .......... and that does not fit thru the doors of the shop! · Mike started on rebuilding the air pump for #428. He has been doing a lot of research on the cross compound air pumps and will look after all of them. He also checked out the valves on 1630's pump which looks to be in good shape after the work done a couple of years back. · Tom continued with machining the shoes and wedges for 428. Above shows one of the shoes that will position the axle boxes in the frame. These are new iron castings as the originals were worn beyond repair. Each must be planed to exact dimensions to enable the eventual refitting of the axles. A slow and tedious process as each axle box requires one shoe and one wedge. So, overall another week of good progress. Nigel Sunday, February 10. 2013Wood Shop Update - February 9, 2013
It seems a lot of folks like to volunteer in the wood shop, another very good turnout with some rare visitors - first timers or members who do not spend all their time in the shop. The event that is becoming space limited is noon around the lunch table - shoulder to shoulder swapping tales, telling stories, and discussing the work.
The biggest job for the day involved making new tongue and groove boards to replace rotted stock inside the MILW X 5000 dynamometer car. Buzz had jointed the new lumber last Wednesday. The next step was to set up the table saw and rip all the wide planks down to about 2 1/8 inches wide That was a lot of ripping but by noon or so, Bill Peterson, Warren Neuhauser, and Dick Melzer are standing in front of a large pile of the slats. We started that job earlier with John Faulhaber also helping, especially with the fences, jigs, and set up on the table saw and soon to be used shaper. Next - the wood was marked for the 'best side' and each was run through the shaper to mill the groove and a small chamfer. All in one pass using our power feeder. The crew feeds, monitors and catches each piece. Not heavy work but many hands to do that and inspect each piece coming off the machines. The second pass through that machine puts the tongue and a chamfer on the other face edge of the boards. We kept the crew busy throughout most of the afternoon. The result was about 450 linear feet of new stock, here being stacked up ready for priming and painting. We purposely kept the tongues shallow as this will be installed on the inside, (concave) side of the car, and each piece will have to be able to create that inside curve. Tim Peters was stripping the many layers of old finish off of one of the doors for Chicago Rapid Transit 1024. He put on quite a show acting as a stripper wearing hearing protection. Those were needed since he was right next to the shaper milling operation which is quite loud. He also ran quite a stack of new basswood planks through the table saw and the planer. This was the first steps to making boards to curve over the roof ends on the 1024. Victor Humphreys applied the first coat of maroon paint to two of the new windows for the Chicago Great Western X 38 and also did more painting on the small quarter round strips for installing the glazing. Not a lot of work on the new doors for the X 38 since the tongue and groove work was a full time process for many hours. But the door joint final fitting came out well under the direction of John Faulhaber, and we did the planing and finish work on the four solid panels which will fill the lower two spaces on each door. It is sitting in the press, ready to be glued up on Wednesday. Lorne Tweed and Eric Lorenz are going over all the details for the the window posts on Cleveland Transit System 4223. While many of these are nominally the same, there are also many for special mounting at the front, rear, or near the side doors. All seem to be measurably different from one another. Dave Fullarton stopped by with a small wood electrical box door, I think he said for the CTA 2000's. Whatever, you can be sure it relates to our rapid transit cars. John Faulhaber and Rich Witt helped and the new door was made in no time while the shaper crew labored on. Dave moved on to painting it at once with GLYPTOL insulating varnish. We will close with the WHAT IS IT quiz of the day. Roger Kramer has a box like dispenser removed from the Ladies Room of one of our heavyweight Pullman Passenger cars. We think it held flat folded paper cups for drinking water, if any of you are old enough to remember those.
|
Blog AdministrationCategory TreeCalendarQuicksearchSyndicate This Blog |
Powered by s9y.
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]