Tuesday, May 28. 2013Wood Shop Update - May 27, 2013
FLASH - We interrupt our regularly scheduled report to bring you this late breaking news. On May 27, 2013 the Chicago and West Towns 141 electric trolley car entered regular public service at the Illinois Railway Museum. The car ran well on our car line route, carrying capacity riders to the delight of our visitors and members alike. The car last ran under its own power in 1947 and represents decades of work by our volunteers and staff alike. FRANK SIRINEK led the project and ROD TURNER, the Electric Car Department Curator, invested time and money, the support of the crew of mechanics, electricians, and restorationists to make this possible. I am sure you will see more news and pics of this event in coming days. Back to your regular programming. The table saw being restored for use in the woodshop is making progress. Here is the restored quadrant - miter gauge mounted on the sliding table. Rich Witt is carefully taking measurements and making a working drawing to construct a set of replica FIRST AID BOXES for our CA&E cars. John Faulhaber is priming many new panels and parts made for our Cleveland Transit System 4223 PCC car. Bill Peterson is using a new paint stripper to remove years of finish on the curved steel panels that once held ad cards in the 4223, while new Board member Norm Krentel looks on. After the paint stripper is done, Bill Peterson cleaned the remnants down to bare steel with a power wire brush. It was not too cold so Bill moved outdoors for this messy step. Paul Cronin, Bob Kutella, and Rich Witt are working on the last set of old ceiling light panels from the 4223. These old fixtures are well and truly mounted with very rusty hardware that fought well for every screw removed. Eric Lorenz pulls out the old rubber gasket that runs along the bottom of each window sash. Amazing that we were able to source new material. It does not go in easily but many more were completed. And the results speak for themselves in this view of the front half of the right side of the 4223.
Sunday, May 26. 2013Steam Department Update 05-25-2013It was one of those days when a lot of effort was required to overcome unplanned events. However, the key objective was achieved. The main objective was to hydro test and then fit the last super heater flue. By 9:30 we had the Sullair running and linked up to drive the test pump and were nearly ready for the test ....... when the Sullair started spluttering and died !. After about 30 minutes trying to understand what was clearly some sort of fuel supply problem, we decided to cut our losses and use the house air to test the flue, although this would not have the power to test the elements at 1000 psi. Good plan, aside from the fact that the house air compressor, which had been running earlier, would not restart as air was drawn !!. Luckily Bob Olson was able to lend us the track department compressor and, by late morning, the hydro testing could begin. Many thanks Bob. During the day teams worked on the errant compressors. After some hours trying to trace a stream of tiny air bubbles, that appeared in the fuel filter, Jerry, Ed and others found and replaced a small brass union nut in the fuel line which had developed a crack, needless to say out of sight at the back !. Richard and others worked thru the control mechanism of the house air compressor. This seems to have been a case of pure bloody mindedness as the pressure switch worked perfectly well after having been opened, examined, adjusted and found to have no apparent sign of any problem !. Maybe it was an air compressor vacation day as the operating streetcar also suffered a compressor problem. So, while teams sorted out the air compressors, the rest of us got back to 1630: · The flue was successfully pressure tested; · We then tested the two super heater elements that failed last year and have been repaired. Both passed the pressure test at 1000 psi. The ball ended mating surfaces, that will be installed into the header, were all cleaned and polished. Dennis completed a couple of additional repairs were to the protective sheets and the elements are now all ready for fitting once the tubes are proved to be water tight; · Eric fitted the copper ferrules for the flue and we then loaded the last flue into position. It was then trimmed to length and rolled into first the rear and then the front tube sheet with no significant problems. ALL THE TUBES ARE NOW ROLLED INTO BOTH SHEETS AND READY FOR TESTING .......... !!. With over 180 small tubes and 16 large ones, all 17 feet in length, we have now re-installed significantly more than a half mile of tube. In celebration of this event there was a major clear out of the firebox and smokebox, which no longer look like storage racks for tube fitting tools ...... but that was after the picture!. · Ed has been continuing the job of cleaning and inspecting fittings from the backhead. One assembly formed of 2 inch heavy pipe and valves, that controls the blower, looked suspect due to pitting in the pipe. We took advantage of having the hydro test system working to pressure test it. This detected a bit of seepage thru the pipe, which also did not sound good when hammer tested. So we decided to make a replacement. Ed, Dennis and Richard were well thru this by end of day; · The main focus now is on the riveting: o Jerry and Mike worked with Dennis to plan and fabricate a steel structure to brace the bucker inside the firebox. There is a considerable trade off here as the frame must brace a very substantial air hammer but must also be man handled onto the footplate and thru the fire hole door into position. There was considerable cussing as this was done but it is now in place; The bracing is designed to support the bucker both front to back (for the rivets in the front of the box) and side to side, when the plate nearest the camera is removed. o We also set up and tested the furnace to heat one of the rivets. Tom had obtained a heat indicating stick (this is wiped on the hot rivet and turns liquid at the required temperature). This seemed to indicate that the small furnace can successfully get a rivet of the required size evenly to the target temperature (although it had cooled substantially by the time I took the picture!); o So the next stage should be to get together the team that will do the riveting and practice the process to ensure that everything can be done smoothly and quickly before we do it with hot rivets. So we have reached one major milestone. While focusing on the riveting, so that we can get the boiler water tight and carry out the first tests, we will now work on a whole bunch of new tasks to start fitting as many parts as we can ahead of the initial hydro test. Work in other areas (aside from the errant air compressors) was limited. However, Mark provided an update on recent work on the CNW #6323 wrecker: · Andy repaired the lower radiator piping and cleaned out cinders and coal from under the deck plates. Since she was converted from steam in 1961, those have been there a while!. · Bill worked on freeing the outriggers; · Nick helped in clearing rigging from the idler car so that the deck can be replaced; · Mike made a new door and doorway; · Phil crawled into the depths to change grease fittings in areas that no one else could get into; · Tom has been working on getting a custom spring made for the boom dog pawl (which stops the boom from lowering unless released). Unfortunately Mark's inspection under the wrecker reveals 2 axles from 1925 and 2 from 1960. The wheels on the 1960 axles are good but those from 1925 are cracked to varying extents. So a search for replacements is now under way. Nigel Thursday, May 23. 2013
CGW X38 Update - May 22, 2013 Posted by Robert Kutella
in Chicago Great Western X 38 Russell Snow Plow at
11:37
Comments (0) CGW X38 Update - May 22, 2013The string of two consecutive good weather workdays was broken yesterday with intermittent rain, some of it heavy. So we worked in the shop and inside the plow body. Buzz Morisette was in the shop fabricating and shaping new framing timbers for the cab cupola on the plow. Most of the wood around the windows and sills was rotted and will be replaced. Dave Rogan worked inside the cupola between downpours and needlechipped and wire brushed a lot of the steel. In an afternoon dry spell he is applying primer here, and then the temporary window blanks were re-installed to help keep it dry. Victor Humphreys and I fussed with the next piece of lining inside the plow. For some reason it was troublesome to fit into place. I bet we went through five fits and they gave us fits. Each time the wood notches seemed to expand (high humidity?) to prevent the piece from slipping in cleanly. With the long piece installed below the side window, Victor quickly marched up the wall toward the right front corner. These are some of the pieces measured and cut last weekend and now ready for nailing. Paul Cronin is just completing the last of 32 more new pieces of interior lining and framing for the plow body. Whoever arrives first on Saturday will have some painting ready for them! |
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Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]