Wednesday, March 18. 2015
556 Coach Update and Other News Posted by Pauline Trabert
in Passenger Car Department at
17:23
Comments (0) 556 Coach Update and Other NewsThis update from the Passenger Car Department was provided by Brian LaKemper... On Wednesday, March 11th, Brian Patterson and Brian LaKemper were at IRM. They managed to wire wheel two of the three needle-chipped panels of the ceiling of the 556; as well as some progress on Dover Strait. Brian LaKemper wire-wheeling a ceiling panel that was needle-chipped late last fall - Photo courtesy of Brian LaKemper A closer view with a little more progress - still over 50 linear feet of ceiling to go - Photo courtesy of Brian LaKemper Unfaded paint was found underneath a car sign warning of extra fees for buying tickets on the train - a chip was used to source the correct color needed to repaint the lower portions of the car - Photo courtesy of Brian LaKemper This is a Pullman ashtray that was disassembled a while ago, Brian L. reassembled it for display in the Dover Strait - Photo courtesy of Brian LaKemper On Saturday, March 14th, Mark Hoffman, Brian Patterson, and Brian LaKemper were working on 556. Mark wire wheeled the third cleaned ceiling panel, and he and Brian P. worked on sanding the sections of the ceiling that were wire wheeled in preparation for primer. Mark planned to prime it on Sunday. Brian L. worked on finishing up the incomplete repairs to the 556's brake system. The repaired brake beam that was installed last fall received brake shoes and was connected to the brake rigging. Phil from the steam shop is owed a HUGE thank-you from all of us in Barn 3 for managing to wiggle himself and tools underneath the car to connect the rigging. After all the rigging was connected, Phil and Brian L. wound down the handbrake to check that the rigging was working again. All was in order, so with help from Greg Kepka, Phil hung the 556's brake valve under the car. Once the valve was attached, air was applied from the Barn 4 supply using a single car air tester to charge the car's reservoir and test the brakes. After 10 minutes of charging, Brian L. opened the tester's brake valve and made a reduction. With a little noise of protest, the cylinder extended for the first time in over 5 years. Due to the dirt and grease involved, no photos of the brake work were taken. Friday, March 6. 2015
The Old Bag and the Silver Beaver Posted by Roger Kramer
in Passenger Car Department at
15:20
Comments (35) The Old Bag and the Silver BeaverAfter all these years of waiting the coach dept is finalizing plans to move CB&Q 1309 located in Denver, Colorado and the CB&Q Silver Beaver located in Madison, Illinois to our museum campus. As some of you might remember, both pieces are complete and are "Q" baggage cars. "What is the big hold up," you ask? It's the usually answer: $ MONEY! Where as, moving lighter weight equipment is less expensive, these two pieces will cost much more than the usuall 3 to 4 thousand dollars each. Yes, acquiring new equipment these days is very, very expensive. Let me first explain the situation behind the heavy weight baggage car 1309. The museum has owned this car since 2002 and has considered moving it a number of times but something always comes up to shove it to the back burner. Now with a renewed excitement we are working on moving this car to Irm. Our largest problem is $. We are considering the possibility of trucking it from the Denver area to Irm. Please consider supporting this acquisition! It's about time to do something with this project! Recently, I asked Brian La Kemper if he had any contacts in the Denver area so that we could have current pictures of the car. His contacts sent us these pictures. They are graciously supplied by one gentleman in the Denver railfan community. His name is Nick Gully and we thank him for his efforts and granting permission to use his pictures. The 1309 will cost more money to move on account of its age, distance from the museum and weight. Please consider a donation to the 1309! Now to the Silver Beaver, and yes, that's its name. Sister cars were named, the Silver Stag, Bear, Buffalo, Coyote and Antelope. Do you see where this train of thought came from? Unfortunately, I do not have any current pictures of the 801, Silver Beaver. This car is also a baggage car but is a completely different configuration. It is a light weight stainless steel fluted car and was built by the Budd Co in 1948 for service on the California Zephyr. As some of you already know the Silver Pony, our Dome coach# 1108, was also built for the California Zephyr. This baggage car will fit perfectly with our Zephyr consist, as well as, our other stainless train set. The Silver Beaver will cost less $ money to move because of its rather close proximity to Irm and the age of the car. The 801 has roller bearing trucks and will be shipped on its own wheels to the museum. Estimates to transport this baggage car range from 5 to 7 thousand dollars! Since its baseball spring training season; Here's the Pitch.....We would like to bring both cars home to Irm before......Before Opening Day or the World Series! That will depend on you, our generous supporters of our museum. To keep these two projects rolling to Irm, please consider donations to the CB&Q 1309 and The SILVER BEAVER. The 1309 would look great on our steam train and the Silver Beaver would look equally magnificent with our Nebraska Zephyr!! Thanks Roger KramerSunday, March 1. 2015
Steam Department Update February 2015 Posted by Nigel Bennett
in Steam Department at
16:54
Comments (2) Steam Department Update February 2015
Unfortunately not the update that I was hoping to be able to write 24 hours ago!.
The steam team has worked steadily thru a record cold February and made good progress, primarily on the Winter work on 1630. The work on the boiler was completed and the objective is to carry out an initial hydro test as soon as possible to ensure that nothing leaks on the backhead where it would be hidden by the refitting of the stoker and footplate. We really need some above freezing temperatures to safely run the heater that brings the water up to a suitable temperature for the pressure test. This has held us up for a week or so but the forecast suggests a “warm” day Tuesday so everything was planned. The tender was filled last weekend to allow the water to reach at least shop temperature. On Saturday the pipework was set up and a start made on filling the boiler.
Unfortunately this revealed that one stay seems to have broken during the process of clearing the tell-tale hole. A steady stream of water was apparent as we filled the boiler. With this stay plugged, we were able to fill the boiler and prove that this is the only stay in this condition. However, we now have a stay to replace. This was something that was not in the plan.
By end of day, Dennis had cut out the cab floor under the engineer’s area, the end of the stay in the firebox was ground flush and the stay cap had been removed. This proved rather reluctant and took a couple of attempts, otherwise we might have got the stay out. Anyway, we are now ready to remove it next week.
Replacing a flexible stay is something we did several times during the overhaul and can be done in a couple of weeks, provided we do not hit anything abnormal. However, it is additional work and means that the target of running Memorial weekend is now in some danger.
In parallel with the boiler work a lot of other work has progressed.
Dennis has put in many hours of work building up the yolk and other parts of the tender draw gear support mechanism. We should be receiving a rebuilt draw gear unit shortly and then the work can begin on making any modifications required to fit this under the tender.
A new pin has been machined for the front coupler pocket. The original was heavily worn. Once new bushes are machined and the support plate, that Dennis has rebuilt, is in place we should have a coupler that sits horizontal rather than sagging as it has in recent years!.
The air tanks are now refitted. This has been a big job as we have fitted new Teflon seals to the ball joints of the tanks. It sounds simple but replacing the very worn seals that have been there for many years can slightly alter the fit of the pipes. There is very little flexibility in large diameter steel pipes!. So in some cases we have had to cut and rethread the pipes to make the correct fit.
The new bush for the connecting rod is now complete and in place in the rod.
Dennis built up the brass on the securing disk. (My mistake. I said last month that the odd one came from a Mikado. Actually it is from a consolidation). Once that is machined we will have all the parts to reassemble the running gear.
However, the first steps at refitting suggest that, with the new bearing in place, clearance will be very tight and it may be necessary to remove and adjust the axle box shoes. Measurements that Jason has made indicate that the shoes are marginally thick and will need to be adjusted at some point. It may be that point is now!.
Work has been proceeding on the replacement of the gland packing on the air operated power reverser mechanism.
After a lot of effort the broken bolt in the smokebox front ring was successfully removed and a new one is in process of being fitted. John Heid joined us and was rapidly at work on this.
When the work on 1630 has relied more on welding and machining, people have been able to do some work in other areas.
Progress has accelerated on the Shay.
The big determinant of how quickly the Shay can be brought into service is whether we can clear the tell-tale holes on all stays behind the frames and motor brackets from inside the firebox. If all the tell-tales can be cleared to the required depth, we then need just to replace a number of stays in other areas that have been identified as bad and can then move quickly to re-tubing the boiler. If any stays need to be replaced behind the motor bracket, then we have a substantial project to remove and refit the motor in order to replace them.
Several people have been working on this as time permits but Phil is now working on the stays 3 days each week and making good progress. A lot of stays have been cleared so far. We all wait with bated breath to see if any prove beyond clearance in the critical areas. We should know within weeks now if we can avoid removing the motor.
Various work has been progressed to allow reassembly to move forward if the stay work is successful.
JD has been locating and preparing the various parts of the running boards.
Brian removed the equalizer air tank and cleaned it in preparation for hammer and hydro testing.
(Brian’s comment on this photograph was very fair!. “You could at least have taken a before shot to show just how much muck I had to remove”). Located under the cab floor, behind the engineer’s footstep this tank gets buried is everything thrown up by the wheels. Good job Brian!.
On 428
The riveting team, led by Stu, has put in several days on the cab. There are a LARGE number of small rivets to be placed but they are progressing and the number of temporary bolts showing on the cab is steadily reducing.
Once it is at temperature the rivet is struck on the anvil to dislodge any scale and then put into the hole.
The bucker holds the head of the rivet in position as Stu uses the air hammer to form the other end of the rivet inside the cab.
Although the basic method is the same, these are far smaller rivets than we had to use on 1630. Rather than fighting to ensure that the rivet is formed while still malleable, the risk with these is more that they can easily be over hammered and have unsightly deformed heads.
The process of Dennis building up with weld and Eric then machining to final dimensions has proceeded steadily thru the many components of the spring rigging. With this now largely complete, work has now started on machining the valve rods.
Mike returned this week after being out of state for some weeks and work restarted on the planer in preparation for the axle box work.
So March looks to be a busy and critical month. Wish us luck!. And if you fancy getting your hands dirty ………!!
Nigel
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Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]