Today was a short day in the shop due to a museum planning meeting taking place in the morning. The plan was to repair the hot water cab heaters in the Illinois Terminal 1605. We're not sure how longs it's been since they've been used since we primarily operate in warm weather. Last year while moving one of the unit coal trains, it would have been nice to have in mid April. Anyway, Mark R and I started on replacing the bad hose couplings between the bottom of the heater cores and the supply and return pipes that run through the floor. The conductors side had one replaced while the engineers side had both replaced.
After replacing the hoses, we checked the motors and found the conductors side not even wired in place and loose bolts holding the motor in place. Dan C joined for a bit to figure out why we didn't have power to the heater breaker, but as it turns out, this GP7 has that wired to the aux gen, so it'll only get power to the cab heat fan motors if the locomotive is running. Jumpering from the battery knife switch temporarily, the motors and switches worked normally.
Next up was to replace a 10 inch section of 1 inch pipe on the cab heat supply pipe that had been removed and plugged. Mark worked on removing the plug and union while I cut and threaded the pipe nipple. The rest went together very easily. While showing Mark where the drains were located, we noticed a 1-1/4 inch union that was disconnected near the rear of the locomotive where the cab heat return line goes back into the engine room. The threads on the union were damaged, so it was removed. We did not have a replacement in stock, so that will be finished in a few days.
Sunday a few of us plan on reconnecting a number of items to the CNW 411 HEP radiator hatch. If anyone wants to lend a hand, we'll be at the shop by 10:30am.
Jamie
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...