The heat this weekend reminded me just how much I like early spring and
late fall... anything over 65 degrees is just too hot. But the high
humidity Saturday didn't stop us from working. The gang this weekend
was Tom H, Steph J, Steve L, myself and special guests JD Marzec, Greg
Frech both from the steam shop and John from the carshop who was
attending for regular membership. As advertised, most of us arrived on
time and prepped for a trip to Four Mile Siding to replace the
switchpoint on the turnout side of the new power switch. We split into
two groups to start out. Steve, Steph and John got the J580 A8
Motorcar, Welding cart and hydraulic cart switched out of Barn 2 while
Tom, JD and Greg got the Model 50 Burro, CNW flat and EJ&E 529
caboose together in Yard 11. I ran around gathering fuel, water and
ice and got the forklift out to load the new switch point onto the
flatcar.
We made it out to Four Mile and were joined by Julie
J and Bob O from the signal dept to replace the point. We made quick
work out of the job and had the new rods on, including the 'new' #2 rod
within an hour. It seems this point is indeed correct and will work
fine. We made the slow trek back to the property a bit after 1PM and
had everything put away around 2PM. I'm glad to report that all of our
machines worked very well and the only thing that required a jump start
was the forklift...sigh
The rest of the day we spent mostly in
Yard 11 cleaning off the C&NW flatcar and continuing to load our
scrap gondola. The old switchpoint was set up near B&G for
Volkmann. JD was able to cut frog bolts with our oxy/ acetelyne torch
making quick work out of that. Everyone did a very good job and I
appreciate all of the help. I think everyone had an enjoyable day but
I've been known to be wrong..
Sunday was only slightly lower
key. Tom, Steph and I made up the Track Dept while Steve L spent the
day helping the Electric car shop in Barn 4. The goal was to cut brush
near Karsten's crossing with the Amtrak brushcutter before operations
got underway. Tom and Steph arrived on time and got the machine out
and on the rail early. After the Electric car shop finished testing of
the overhead on the main it was our turn to get on the line. I showed
up just as they were finishing up the first section of cutting and just
as the machine developed an air leak... An old air line under the
machine came loose from its fitting which put us out of service on the
main until we could come up with a fix. An hour or so later, after
numerous trips to the property and failed attempts at a repair we ended
up changing the entire hose. We got ourselves back in service and
cleared the mainline for revenue service shortly after. There is still
a little bit of cutting left to do near Karsten's but the worst area
has been taken care of. It was a warm weekend and proved how important
it is to carry water with us on the line. We have a cooler in Barn 2,
lets remember to keep it full.
In the next few weeks we will
need to take care of some housekeeping chores. The fire inspector will
be coming soon and we have a list of things to clean up ASAP. All of
the plastic hanging from the ceiling in Tk24 will need to come down and
the aisles need to be clear.
Until next time...
Adam Robillard
Roadmaster
lzeje657@msn.com
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]