A successful day at the steam shop.
We now expect the ultrasonic testing to be done weekend of May 5th so yesterday was an opportunity to progress other activities in preparation. 1630 saw the light of day for the first time in nearly a year when we pulled her out to remove the throttle valve and allow cleaning of both the locomotive and the shop area where she has been sitting.
Eric and his father made good progress in testing the tell tale holes in the firebox stays. The engineer's side is now largely complete. By midday Jeff had the BrownHoist de-winterized and running and we were ready to shunt 1630 out of the shop.
Once outside we worked on the removal of the throttle body, which will be lapped to ensure a good seal when reassembled.
This is an awkward piece that sits in the dome.
However, with some help removing cotter pins from inside the boiler, it was removed and taken to the shop. It has apparently been removed and refitted in the past with all the tubes in place. I have a lot of respect for the guys who achieved that !!.
It was good to see 1630 in steam again !!.
Seriously though, it was an opportunity to do some steam cleaning and the locomotive now looks a good deal better and easier to inspect.
The opportunity was also taken to clear the area around and under the locomotive, that had accumulated the most amazing collection of insulation debris and other muck as well as odd items that had fallen while working.
By end of day she was back in the shop and ready for ultrasonic testing.
In other areas, Paul and the lads made good progress on needle chipping and wire brushing the Shay truck. Glenn over came a problem, that has developed in recent weeks, of the fork lift battery failing to hold a charge. Far from the suspected defective battery he found that a loose terminal and blown fuse in the line from the alternator meant the battery had not been connected to the charging system at all for the last few weeks!!.
Next weekend will probably be quiet as many of us need to attend the rules exam.
Nigel
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...