It was a day of downs and ups in the steam shop. The order is significant, despite a couple of early set-backs it became
a very successful day. I had to leave mid-afternoon
for an evening event downtown. The major
progress was achieved in the evening ..... hmm, there may be a connection there
!!.
We keep pushing
forward on 1630.
·
When we arrived in the
morning, Dennis had completed the required welding during the week but no more
rivets had been placed. It turned out
that a couple of the mid-week team had been sick or unavailable so no riveting
was possible on Wednesday.
·
In addition Kevin
had been in during the week and made great progress on needle chipping the
front of the locomotive ready for repainting.
In addition he had done a lot of cleaning in the shop. This is a major part of work in the steam shop. A lot of what we do creates dust and, without
periodic cleaning, the place gets into a real mess.
·
We are now getting
close to the first tests with water in the boiler to check the sealing of all
the tubes that we have fitted. So
various jobs were scheduled to prepare for this. One big requirement is obviously water, which
we need to supply from the treatment plant in the steam lead and have available
for use in the shop. For this we use the
tankage of our milk car.
Jim
West, who was conductor of the day, managed to schedule things so that the car
was switched over to the steam lead by the service locomotive before the first
train. Thanks Jim.
Thereafter
things went downhill !. We initially had
problems with leakage from the inspection cover of the pump in the boxcar. Good thing it was near 90 degrees as a number
of us had unexpected showers. Then,
having overcome this and linked the milk car to the supply, we discovered that
two key valves in the milk car were split.
It seems that the car was not completely drained last Fall and the
valves froze. Good thing we started this
a little ahead of when we absolutely need the water for testing.
During
the day Jeff removed the damaged valves from the car so that replacements can
be ordered for fitting next weekend. Stu
and Jeff worked on the water treatment plant so that the softener, which was
out of commission due to a leak, is now working again and properly sealed the
inspection cover on the pump to avoid further showers.
·
Rick, Paul and
others worked on the smokebox front, cleaning this up and preparing the gasket.
·
Eric continued work
on the super heater flues in the front tube sheet. He is ensuring that any excess ferrule is
removed and starting to flare the tube ends in preparation for beading the ends
once we have ensured that they are water tight.
·
Several of us worked
on fitting the plates in the cab, on which the gauges are mounted, and then
fitting the boiler pressure gauges to these.
The water level gauges were also fitted.
All of these are needed for the initial hydro testing. It is really nice to see fittings coming back
into place on the back head, which has been bare for more than a year.
The pressure and
water gauges are now back on the fireman's side
and on the
engineer's side as well.
·
Then, after I left,
the main event started. The three
remaining rivets were placed. THE
RIVETING IS COMPLETE. Some of them still
need to be caulked but the riveting itself is done. The next key job is to fit the two flexible
stays. The stays fit into the two open
sleeves that can be seen just above the rivets in the front face of the firebox
wrapper.
So another major milestone is achieved. The patch is now fully installed and we can
move forward to testing and reassembly.
Nigel
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]