Sunday, July 7. 2013Track Department updateSaturday's gang completed work by 10AM... but I'm getting ahead of the story.
A plan was hatched to get the gang together Friday night and go out to spike and plate. Marcus arrived way early and was out plating from around noon to 4 with Bob Olson. Around 6 the gang changed to Marcus, Mark Gelman, Mark Riemers, with a special guest visitor Bobby Ryan, and myself. First we loaded the last 12 kegs of spikes into the spiker ... just in case, and then headed out onto the main setting up an out of service at East Switch. We got out just in time for the Switch Fest 2013 to begin prep for the Trolly parade. We went out to where Bob and Marcus left off plating, and set to work. Mark Riemers started spiking the north rail and working his way back west, while Marcus and Bobby Ryan ran the plater, working East. Mark Gellman and I set plates and cleaned out cribs for the jaws of the plater to grab the rail. We worked till almost 10PM when we ran out of light. Somewhere towards the end Mark Riemers turned the spiker on the wye. We tied up for the night, with Bobby heading to his hotel in Rockford, Marcus going to pick up Gwen, and Mark, Mark, and I going to Joes for dinner. Saturday Morning, The plan... Finish the job. Start time 05:30 We tied down the machines on the main in our out of service Friday night, so it was simply fire up and go to work. And work we did. We were slightly better equipped for the cribbing job, having grabbed a couple picks and the job went well. Mark went back to spiking - South rail this time, Mark Gellman, and Marcus ran the plater, and were helped when Bobby Ryan joined us again, and I went to cleaning cribs. Mark Riemers helped with cribs when he caught up with the spiking. As we reached the end of the work, I also did some tie crane work stacking the dead wood for pick up later. In the end we completed work, picked up the plater and put it back ont he flat, and ran back to our OOS limits. On the way Bill Lygiros was found to be stacking old spikes as he walked in from Karstens. I think we surprised the dispatcher by showing up before being called to clear up. We were in 24 track long before the first revenue train left. He also left with a great deal of relief on the slow orders. Thanks to the final push by the gang, we picked up two slow orders, annulled one line of the Summary GO, and gave them a railroad they can run on. Only one slow order remains, and that is due to the swerve left over from the tamper losing it's mind. I'm working on a plan to go out one evening with the a loco and use jacks to smooth out the dipsy do, and air tamp the ties to get that last slow order off. After the paperwork, and anulling the bulletins with the dispatcher, the crew was off to breakfast at Dino's... Of course the RR gods could not let us accomplish this much without their games. As I was rolling into 24 track with the tie crane, she lost power and started smoking like an Alco going from start to run 8. It was discovered the Temporary fix of the air box intake pipe had failed, getting partially sucked into the intake. Mark Riemers delicately ripped it off the machine, and replaced it with the proper flex steel pipe we picked up later from Napa. A new battery was also picked up for the hydraulic power pack and a new battery terminal crimped on. JD is still working on a replacement hydraulic hose to replace the one that was damaged when it shorted to the battery. Marcus
and Bobby were the Car line dispatchers from the tail track switch to
the S curves for helping put away the fleet. No small task to be sure.
I can honestly say, I have never seen barns 6,7 and 8 so empty before
in my time at IRM! So
Nice work this week IRM Track crew! Job well done. We now move to
the clean up phase of the project. picking up spikes, spiking up the
last few ties on the north rail due to submarined ties, and then
regulating. Frank D. Sunday, July 7. 2013
Steam Department Update 07-06-2013 Posted by Nigel Bennett
in Steam Department at
19:23
Comments (9) Steam Department Update 07-06-2013
A brief update courtesy of Phil as I was not at the steam shop this weekend.
On 1630 a major milestone is achieved. The firebox corner that was the cause of her withdrawl from service is now completely restored.
· The stays were fully fitted, cut to length and then formed with the air hammer. They can now be seen fully fitted into the patch and ready for service;
· Jason instructed Collin, Phil and others in the use of the gauge testing equipment. The boiler pressure gauges were successfully tested and can now be finally fitted in the cab;
· Phil and Jerry carried out a tricky "fishing exercise" and managed to extract two ferrules that had dropped into the bottom of the boiler barrel during tube fitting. Not absolutely essential but a great deal better that they are not loose in the bottom of the boiler;
· Work is progressing on refitting the remaining flexible stay caps were loose following removal for inspection and cleaning of the stays;
· Brian, Paul and David made good progress on stripping the air tanks.
Meanwhile Bob is starting to install the ducting to provide a permanent power supply to the planer.
.............. and lastly a reminder. IF YOU DO NOT ALREADY HAVE YOUR TICKETS FOR THE STEAM DEPARTMENT BENEFIT next Sunday (14th) at the San Filippo Estate- THERE ARE STILL A FEW AVAILABLE. They can be booked from the link the IRM website. Hope to see you there.
Nigel
Sunday, July 7. 2013Wood Shop Update - July 6, 2013Here is my nomination for the best before and after photos of 2013. On the left is one of the cab/cupola seats from our Chicago Great Western X 38 snowplow. On the right is its mate, with restoration complete. WOW! You last saw a pic of this two days ago as we were working on the frame. Hardly any time went by and our upholstery guru, John Mc Kelvey, has it done!! We continue to work on the restoration tasks for the plow but perhaps are a month behind our plan for the exterior re-painting. Due to rainy weather maybe six of the last eight weeks. So you have seen related work like the above seat restoration and a lot of work to restore the interior of the plow. STUNNING or SUNNING?? This is a shot of Cleveland Transit System 4223 which came out of Barn 4 for a static display on this day of our largest Trolley Pageant ever. Those of you who have followed along for years, or happened to walk by it in our work barn, can clearly see the transformation and the possibilities for moving the work forward. This is another short report since we did put on a show with the pageant, something of the scope never before attempted at IRM or any other Museum in the USA. There had to be over 50 volunteers involved in the effort, many for several days or weeks of work. For my part I operated the Sand Springs 68 along with crew members Bob Sundelin and Paul Cronin. Thanks to both for their efforts. In addition to the many crew members needed on the equipment there was a large contingent of volunteers working behind the scenes to make this come off smoothly, staging, throwing switches, make it look seamless to the visitors. In case you did not see it in person, too bad. But our MEGA EVENT weekend focused on electric cars continues. It is not too late to visit today, tour the iconic Electroliner, and witness and ride many trains of the Chicago North Shore and Milwaukee. See you there. |
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Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]