Wow!. The Winter
temperatures have certainly arrived with a bang this year. This time last year we were happily moving
tubes in from the boxcar. This weekend
anything outside was done quickly and in heavy clothing. At 20 degrees with a strong wind most work
was done inside.
However, we did manage to ensure that the drop pit pump and
anti-frost heating are working and move the Sullair into the shop so that it
should start if required.
On 1630:
·
Matt and Jim produced new washers for the water
connections between the tender and the injectors. The filters baskets were passed to Dennis to
work on the brazed surfaces. Hopefully
the combination of these two actions will provide a long term fix for these
connections that have tended to leak for some years.
·
Rick made good progress on fitting the sheet
metal screws to secure the radius pieces of the sheet metal on the back
head. Once this and a couple of other
jobs are done we should be able to paint the firebox in the cab. That promises to be great fun working around
all the pipes and fittings!.
·
Eric did some hours of laborious needle chipping
to remove paint from the driving wheels.
Kevin did a lot of this some months ago.
Now that the locomotive is in a different position, the rest of the
wheels can now be cleaned off ready for painting.
·
Ed and Bob remade the copper pipe connection for
the steam heat line;
·
Matt refitted the reflectors to the gauge lights. These should now be a lot brighter;
·
The last of the three air tanks below the
walkway was removed for painting. In
addition, I worked with Collin and Matt to remove the small equalizing
reservoir from under the cab floor so that it can be hammer and hydro
tested. This is small but a real pain as
it is surrounded by a bunch of pipes that run just below the cab floor. In the photograph below you can just see the end
of the reservoir in this view under the cab on the engineer's side.
Here Collin is squeezed between
the locomotive and tender working on the nuts that secure the reservoir to the
back of the locomotive.
Anyway, after much cussing and
tricky maneuvering, it was extracted. By
end of day, I had successfully hammer tested and primed it.
·
Jerry made good the insulation on the fireman's
side, that was removed to fix the leaking lubricator line. He then started on the lagging of the firebox
side sheets. These are unusual when
compared to all the other insulation. As
they need to be removed annually to inspected the firebox side stays, the
insulation is attached to the sheet metal rather than the boiler;
·
Dennis continued work on the sheet metal for the
smokebox.
·
Cameron and Brian worked with Tom to machine the
new stud.
In other areas:
·
Phil prepared the bolster of the Shay by
removing the last loose spring locator.
Once Dennis welds in the new locator we can start planning to put the
bolster and springs back into the truck.
·
Tom completed machining the first wedge for the
axle boxes on #428;
·
Brian and Cameron continued drilling the brake
hangers for #428;
·
Cameron worked on the moulds that are required
for the casting of the babbit bearings for the cross heads;
·
Bob and Ed worked on preparing the oil system of
the planer for filling. The challenge is
the best way to get debris out of the system before filling it with the
approximately 80 gallons of oil with which it will operate;
·
Brian brought in the replacement switch for the
forklift and this was fitted.
So it was a successful weekend as we continue to work thru
the Winter maintenance tasks. Next
weekend will provide a good opportunity to work off the effects of the turkey
!.
Happy Thanksgiving
Nigel
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]