Sunday, November 24. 2013
Steam Department Update 11-23-2013 Posted by Nigel Bennett
in Steam Department at
13:39
Comments (0) Steam Department Update 11-23-2013Wow!. The Winter temperatures have certainly arrived with a bang this year. This time last year we were happily moving tubes in from the boxcar. This weekend anything outside was done quickly and in heavy clothing. At 20 degrees with a strong wind most work was done inside. However, we did manage to ensure that the drop pit pump and anti-frost heating are working and move the Sullair into the shop so that it should start if required. On 1630: · Matt and Jim produced new washers for the water connections between the tender and the injectors. The filters baskets were passed to Dennis to work on the brazed surfaces. Hopefully the combination of these two actions will provide a long term fix for these connections that have tended to leak for some years. · Rick made good progress on fitting the sheet metal screws to secure the radius pieces of the sheet metal on the back head. Once this and a couple of other jobs are done we should be able to paint the firebox in the cab. That promises to be great fun working around all the pipes and fittings!. · Eric did some hours of laborious needle chipping to remove paint from the driving wheels. Kevin did a lot of this some months ago. Now that the locomotive is in a different position, the rest of the wheels can now be cleaned off ready for painting. · Ed and Bob remade the copper pipe connection for the steam heat line; · Matt refitted the reflectors to the gauge lights. These should now be a lot brighter; · The last of the three air tanks below the walkway was removed for painting. In addition, I worked with Collin and Matt to remove the small equalizing reservoir from under the cab floor so that it can be hammer and hydro tested. This is small but a real pain as it is surrounded by a bunch of pipes that run just below the cab floor. In the photograph below you can just see the end of the reservoir in this view under the cab on the engineer's side.
Here Collin is squeezed between the locomotive and tender working on the nuts that secure the reservoir to the back of the locomotive. Anyway, after much cussing and tricky maneuvering, it was extracted. By end of day, I had successfully hammer tested and primed it. · Jerry made good the insulation on the fireman's side, that was removed to fix the leaking lubricator line. He then started on the lagging of the firebox side sheets. These are unusual when compared to all the other insulation. As they need to be removed annually to inspected the firebox side stays, the insulation is attached to the sheet metal rather than the boiler; · Dennis continued work on the sheet metal for the smokebox. · Cameron and Brian worked with Tom to machine the new stud. In other areas: · Phil prepared the bolster of the Shay by removing the last loose spring locator. Once Dennis welds in the new locator we can start planning to put the bolster and springs back into the truck. · Tom completed machining the first wedge for the axle boxes on #428; · Brian and Cameron continued drilling the brake hangers for #428; · Cameron worked on the moulds that are required for the casting of the babbit bearings for the cross heads; · Bob and Ed worked on preparing the oil system of the planer for filling. The challenge is the best way to get debris out of the system before filling it with the approximately 80 gallons of oil with which it will operate; · Brian brought in the replacement switch for the forklift and this was fitted. So it was a successful weekend as we continue to work thru the Winter maintenance tasks. Next weekend will provide a good opportunity to work off the effects of the turkey !. Happy Thanksgiving Nigel Monday, November 18. 2013
Steam Department Update 11-16-2013 Posted by Nigel Bennett
in Steam Department at
22:04
Comments (0) Steam Department Update 11-16-2013This weekend we started in earnest on the over winter work program, primarily on 1630. The biggest overall job will be painting the locomotive. Brian and Jane worked on understanding exactly how best to apply the paint that will be used. It is a two part type that we have not previously used and some significant planning and preparation is required. Two of the air tanks were removed and these will be the first items to be painted to provide experience and testing of the best methods of preparation and application.
Dennis was hard at work on the plate work and mesh screens for the smokebox. These are now approaching completion.
We also worked thru the items that we needed to do while we can still pressurize the boiler. · One key item that worked out well was the tracing of a small steam leak that appeared around the handrail stanchion juts behind the sand dome. Steam appearing from behind the lagging is always troubling as it can indicate all sorts of things, some more troubling than others. We had suspected (and hoped) that it might be as simple as a loose connection on the lubricator steam line. Much to our relief it was found that this was exactly what it was. After removing a good deal of sheet metal and lagging to locate the union, soap solution revealed a very obvious leakage where the union had not been fully tightened when a new pipe was fitted.
· Matt, Jerry and others worked on the cab lighting. 3 lights in the cab were not working during the test running. A mixture of defective bulbs and a loose connection were found and by end of day, all lights on the locomotive were fully operational when the generator was run on air. They did also find and correct the issue of "dim" gauge lighting on the engineer's side!. The lights sit in little dishes that direct the light toward the gauges. The dishes have a white enameled surface to direct the light. The years have reduced this thru rust and smoke to a nice matt black!!. Cleaning and repainting have fixed that issue. Jason, Cameron and Phil spent much of the day winterizing the water supply in the boxcar. This is a tricky job involving a lot of blowing compressed air thru the system to ensure that it is water free and then taking apart the water softening system. The weather did not help with wind and rain making the job more unpleasant than usual. Good job guys!. So it was a successful day working toward having 1630 in top condition for 2014 operations. Nigel
Tuesday, November 12. 2013
Steam Department Update 11-09-2013 Posted by Nigel Bennett
in Steam Department at
10:34
Comments (2) Steam Department Update 11-09-2013It is a rather brief update this week. I made it back to the shop on Sunday after spending Saturday travelling back from New Zealand. A lot of activity was apparent from Saturday and continued on Sunday. After a week, 1630 no longer looks like an operational locomotive. The main activity on Saturday was to thoroughly drain her and then winterize (primarily running on air to blow any residual water out of the system). A number of parts have been removed to facilitate work over winter. This is not unexpected. The intent had always been to carry out test running to identify anything that needs to be dealt with as maintenance activity during the winter. The main objective of my trip to Union on Sunday was to work with Brian Davies before he leaves to produce a full list of work identified during the test running. While there is nothing particularly threatening it is a long list that will keep us busy over winter. The work also needs careful planning as, for example, it is important to deal with everything that may require us to pressurize the boiler to allow testing before we move on to things that require removing items that allow air to escape from the boiler !. The boiler lagging already looks substantially less complete. The securing bands must all be removed to allow painting of the sheet metal and this was started on Sunday. Visitors to the shop will notice that the end covers have been removed from the valve chambers. It is not planned that work will be done on the valves this winter but it was apparent during running that the valves are leaking significantly. While this is not essential for 2014 running, we will measure everything up for ring replacement perhaps in the following winter. On Sunday, Brian was removing the air tanks for painting while I worked on removing sheet metal and insulation to locate a small leakage of steam from the lubricator heater line along the boiler. In other areas, Tom, Jim and Cameron were working on the brake shoe holders for #428. The first of these was test fitted and looked good. So work started on the remaining 7. Mike was working on the plumbing for the planer. This is an interesting 3 dimensional jigsaw puzzle with a number of copper pipes, all with the same size connections, coming out of the hydraulic system into the machine. Now is a very good time to reflect upon how nice it would have been if someone had taken some good photographs of the set-up 20 odd years ago when it was taken apart !. So if, like me, you missed seeing 1630 as a hot steaming machine last weekend, it will be some months before you will be able to see her even looking complete again. However, the feel in the shop is very different. After two years fighting toward the objective of a working steam engine we now have one and must tackle the various winter maintenance tasks to make reliable operation the normal routine in 2014. One further important piece of information – SAVE THE DATE - The 2014 Steam Department Benefit at the Sanfilippo Estate will be on Sunday 29th June 2014. Nigel |
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Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]