Saturday provided a brief respite from the recent frigid weather in
which the Winter work plan could be continued steadily.
On 1630;
The large copper pipes were annealed. Dennis heated them to red heat with the acetylene
torches and then Brian and I moved them into the water bath to quench
them. They are now ready to be
re-insulated and then re-installed when the painting under their positions has been completed;
Jane and Stu finished painting the backhead in the cab;
Jane, Ed and I were busy preparing the front and
walkways of the locomotive for painting;
Brian, Jerry and Jim worked with Tom on the plans
for painting. More advanced spray
equipment is needed for the paint that has been donated for this repaint. This will hopefully be available in the next
couple of weeks and the first test spraying can then be planned;
We took the opportunity to get out to the boxcar and
measure the dome cover in order to determine how thick the insulation on the dome
should be. With this information, Jerry
will hopefully be able to complete the insulation. The dome is the last piece remaining to be
insulated;
The small air tank that serves as the reservoir for
the reverser was painted with conventional spray paint to allow it to be
refitted. This is required to allow the
reverser to be moved allowing measurements of the valve chambers for future
fitting of replacement rings.
In other areas:
Phil put in a solid day with the air hammer
caulking the tube sheet rivets on the Shay.
This is hard and essential work ensuring that the head of the rivet is
tightly sealed into the boiler barrel.
With eight rivets to do, Phil was working with the air hammer for much
of the day and most other people in the shop were wearing ear protectors!;
A team including Jim, Jerry, Matt and others fitted
the wires to #428 that will be used to attach the insulation. This is not an indication of an immediate
start to insulation but rather reflects the fact that, since the boiler is
currently bare, it is easier to install these wires before pipe work is fitted
along the boiler;
Work on the planer suffered a set-back. Having filled everything with oil, an initial
attempt was made to test the hydraulic pump.
The good news was that the pump certainly develops pressure. The bad news was that it was immediately sufficient
to blow a gasket in the hydraulic control assembly. Investigation is now under way to determine
why this is not sealing correctly.
So the work continues steadily at the end of another year. It is certainly good to be able to compare
where we are now to where we were at the end of 2012.
Happy New Year,
Nigel
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...