On Saturday March 19th, our plan for the day was to remove the radiator hatch from IT 1605 and replace a bad core. Our day started a little after 9:00am with Jeron G getting the CE 15 running as I started clearing a work area on the North aisle of the shop by the door and clearing some material stored by the pallet with the new core. We were joined by Mark S, Lee E, Don P, and later in the day Matt O joined in. We moved the string of locos out of the shop working with the track department who was also using the Forklift and prepping machines for their days work.
Sometimes, like this, it is nice having a big Cat forklift that can lift a lot and has forks that can go some 20 feet high. Although it can be too large for some uses, this wasn't one of them. We had the hatch off in a few minutes and Mark and Jeron began taking some steel plates the edges of the radiator cores. We had the right bank of cores out within a half hour after that. After we moved them to the work area in the shop, it took a little under two hours to unbolt the cores, chase the threads and clean all the bolts, make a slight modification to the headers on the new core, and bolt it all together with new gaskets. We took a break for lunch before placing the cores back into the loco.
After lunch, we moved the new bank back to the west end of the shop outside and lifted them back into the locomotive. Just a few slight adjustments were needed to line up everything. The air deflectors were screwed back into place, modifying a couple of them where the new core was sitting. The hatch was placed back on and bolted down. Lee and Don even had time to start inspecting the main and aux gens, and fuel pump motor. We cleaned up tools and supplies, put the locos away, and were done by 6:00pm.
Our next job over the next week or two will be to bolt all the water pipes back on, finish the inspection, and fill here with water and test everything out.
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...