Tuesday nights work on the Green Bay and Western 2407 was to fix more leaks on some of the water pipes. Jeron Glander, Dave Fullarton, and myself arrived about 6:30pm and spent about four hours working on it. We started in the cramped quarters of the radiator room, using the porto-power to move one of the main water pipes around, bending a mounting bracket straight again and getting 3 main points of the pipe to line up properly. After a lot of adjusting, the sleeve fit perfectly. Then Jeron and Dave wire wheeled the surfaces of the pipe where the rubber gaskets of the coupling will seal and then reassembled the coupling and tightened up all the clamps.
After that I removed a small 1/2 x 8 inch pipe that was cracked, removed the reducing bushing that had the broken portion of the pipe stuck in it, removed the broken portion and replaced with a new pipe. Naturally, it has to be in one of the worst spots to reach, between the oil cooler and main water pipe, blocked by the drive shaft and eddy current clutch and guards, but we were able to squeeze in there and get it done.
Dave did some vacuuming of some debris on the floor before he and Jeron moved on to the engine to start taking off some water elbows between the head and block. There are a number of gaskets on the engine and air compressor that are dried and split and just need to be replaced.
I have created a photo gallery of the mechanical work as it progresses. There are also a few photos of the cab and the fogged and bad windows that need to be replaced. These will all have to be replaced with FRA glazing, donations to the RSD15 would be greatly appreciated and will assist in the costs of the restoration.
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]