This was a big day at the steam shop. All activity was focused on 1630 and the
first testing of the boiler completely full of water and under some pressure.
It is a fairly lengthy process to set the boiler up for
pressure testing. The boiler and water need
to be fairly warm (about 100 F) for testing. So aside, from pumping 2500 gallons of water
from the milk car to the boiler, there is about 5 hours of circulating the
water thru the gas fired pool heater to bring the whole system up to an even
temperature.
Starting in the morning it was late afternoon before the
whole system was at temperature. During
that time we spotted and corrected minor leaks around the inspection and dome
covers.
Removing the dome cover to fix the seal gave this
interesting shot into the open dome. The
boiler is now about as full of water as it can be.
With everything sealed we started to apply pressure to check
for leaks. In general, we were fairly
pleased with the way that the work we have done stood up to pressure. There were maybe 20 small to tiny leaks disclosed
around tube ends. In retrospect one
mistake was that we did not fix leaks around two super heater flues in the
front tube sheet. These were very small
sources of drips under gravity but became the limiting factor when we reached
150 psi.
The firebox patch was tight aside from a small spot in the
caulked joint with the mud ring which showed a slight leak at 150 psi. This should be easily fixed by a little more
caulking. A couple of rivets close to
the patch showed signs of weeping. This
is not surprising given the expansion and contraction associated with the
welding and can be fixed by a little work with the caulking hammer.
The nuisance and minor setback was an area that we had not
worked on. We found tiny pinhole cracks
in the sockets of two flexible stays in the back head. These may have been there when she last ran
as they are so small that we would probably not have seen any leakage from
under the lagging and jacket. Certainly
they would not have caused any loss of pressure in the hydro-testing.
However, knowing that they are cracked, even a pinhole, they
must be replaced. This involves grinding
off the inner end of the stay and, after heating the end of the stay, trying to
unscrew the stay from the socket. If this
fails you have the much more time consuming job of drilling out the stay at the
inner end. However, it worked well. By Saturday evening both stay bolts were out,
without the need to drill either. In
this view you can see the empty sockets after the stays were removed.
On Sunday I started cutting one of the sockets off from the
back head and, in the afternoon, Mike and Tom completed the job. So both of the sockets shown above are now
gone and we are ready to fit the new sockets.
Tom will then need to drill and thread two new stay bolts so they can be
refitted. This will mean no pressure testing
next weekend but hopefully all will be back and the leaks fixed by 8/10.
On this basis, I met with the FRA inspector on site Sunday
and we scheduled the formal hydro test for 8/18, subject to a successful second
stage test for leaks the previous weekend.
Just about all effort was concentrated on 1630. However, a big event was that both Bill Chyna
and Glenn Parkhurst visited. Glenn for the
first time since his motor cycle accident in May. Glad to say they were both in good form and
Glenn is hoping to be able to join us again when he has his prostheses fitted
in the next few months.
I am heading for the UK on business this week and will not
be around the shop next weekend. So I am
hoping to see a lot of progress when I get back in two weeks time !.
Nigel
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...