This was a big day at the steam shop. All activity was focused on 1630 and the
first testing of the boiler completely full of water and under some pressure.
It is a fairly lengthy process to set the boiler up for
pressure testing. The boiler and water need
to be fairly warm (about 100 F) for testing. So aside, from pumping 2500 gallons of water
from the milk car to the boiler, there is about 5 hours of circulating the
water thru the gas fired pool heater to bring the whole system up to an even
temperature.
Starting in the morning it was late afternoon before the
whole system was at temperature. During
that time we spotted and corrected minor leaks around the inspection and dome
covers.
Removing the dome cover to fix the seal gave this
interesting shot into the open dome. The
boiler is now about as full of water as it can be.
With everything sealed we started to apply pressure to check
for leaks. In general, we were fairly
pleased with the way that the work we have done stood up to pressure. There were maybe 20 small to tiny leaks disclosed
around tube ends. In retrospect one
mistake was that we did not fix leaks around two super heater flues in the
front tube sheet. These were very small
sources of drips under gravity but became the limiting factor when we reached
150 psi.
The firebox patch was tight aside from a small spot in the
caulked joint with the mud ring which showed a slight leak at 150 psi. This should be easily fixed by a little more
caulking. A couple of rivets close to
the patch showed signs of weeping. This
is not surprising given the expansion and contraction associated with the
welding and can be fixed by a little work with the caulking hammer.
The nuisance and minor setback was an area that we had not
worked on. We found tiny pinhole cracks
in the sockets of two flexible stays in the back head. These may have been there when she last ran
as they are so small that we would probably not have seen any leakage from
under the lagging and jacket. Certainly
they would not have caused any loss of pressure in the hydro-testing.
However, knowing that they are cracked, even a pinhole, they
must be replaced. This involves grinding
off the inner end of the stay and, after heating the end of the stay, trying to
unscrew the stay from the socket. If this
fails you have the much more time consuming job of drilling out the stay at the
inner end. However, it worked well. By Saturday evening both stay bolts were out,
without the need to drill either. In
this view you can see the empty sockets after the stays were removed.
On Sunday I started cutting one of the sockets off from the
back head and, in the afternoon, Mike and Tom completed the job. So both of the sockets shown above are now
gone and we are ready to fit the new sockets.
Tom will then need to drill and thread two new stay bolts so they can be
refitted. This will mean no pressure testing
next weekend but hopefully all will be back and the leaks fixed by 8/10.
On this basis, I met with the FRA inspector on site Sunday
and we scheduled the formal hydro test for 8/18, subject to a successful second
stage test for leaks the previous weekend.
Just about all effort was concentrated on 1630. However, a big event was that both Bill Chyna
and Glenn Parkhurst visited. Glenn for the
first time since his motor cycle accident in May. Glad to say they were both in good form and
Glenn is hoping to be able to join us again when he has his prostheses fitted
in the next few months.
I am heading for the UK on business this week and will not
be around the shop next weekend. So I am
hoping to see a lot of progress when I get back in two weeks time !.
Nigel
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]