It has been a really busy week for me at the museum hence a
rather late blog update!!.
I spent Wednesday at the steam shop with Phil and Ed. The main focus was on sealing all significant
leaks at the tube ends that showed when the boiler was filled with water. By end of Wednesday we were to the point that
, when filled well above the crown sheet, we had only minor dribbles and drips.
Saturday was a normal and fairly successful work day at the
shop and Sunday I spent working with the Jim West and the Operations Department
on switching for the Diesel Days event.
So the blog is a little late this week !.
So what happened Saturday at the steam shop?. Overall a great deal was achieved although there
was one set back which meant that we were not able to get as far as our most
ambitious targets.
On 1630 I guess I had better try to answer one question I
was asked a lot at the event on Sunday - when will you be hydro-testing the
boiler?. The answer has to depend upon
what exactly you mean by hydro-testing.
As the pre-requisite for moving on the steam testing we must demonstrate
that the boiler can be pressured using heated water to 125% of operating
pressure (so 225 p.s.i. in our case) and sustain that pressure with minimal
leakage for a period. Our current
expectation is to reach that point in about 3 weeks. However our path to that involves using
water, at first simply filling the boiler, then applying increasing pressure to
identify and test the correction of any leakage. This is the process that we are currently
following. On Saturday our objective was
to finally seal any leakage at the tube ends on simply filling the boiler and
then seal the boiler to allow some pressure to be applied.
·
Following on from the work that Phil and I did
on Wednesday, a team including Phil, Collin, Eric and Sean took it in turns to
identify and seal the last little leaks that showed by carefully rolling the
identified tube ends slightly more. This
was hard and tedious work but, by early afternoon, the tube ends appeared to be
dry with the boiler full of water.
·
Dennis annealed the copper sealing rings for the
two covers.
·
In parallel with this one team worked on
cleaning the threads of the studs that attach the dome cover and another on
fitting the cover of the inspection hatch.
These are the last two components required to seal the boiler and allow
pressure to be applied.
·
All seemed to be going well until one of the
studs securing the inspection hatch sheared off during tightening.
Luckily everything seems to be
shaping up well on replacing the stud.
Dennis was in the shop and did a great job of welding a nut onto the
broken stud and, to our great relief, this stood up to several of us pulling on
a large wrench and the stud unscrewed from the seating. In this view you can see the broken stud with
the nut welded onto it.
This was very good news as the
alternative, had it failed to extract, would have been to grind it flush and
drill it out, potentially a day's work.
The studs screwing into a boiler are quite unusual. The thread into the seating is tapered and
must be specially machined. However, by
end of day, Tom, Cameron and Bob had substantially machined the new stud and,
when I dropped by on Sunday, work was progressing. We should have it replaced ready to fit the
cover next weekend.
·
With the stud out, work focused on fitting the
dome cover. This was the first time that
we had used the new boom for the forklift, which was made with this type of
lift in mind. It was highly successful. The cover was lifted by the forklift in the
shop and placed fairly easily.
It was then tightened down without
issue. This was a great deal easier than
the previous method that required the locomotive to be pulled outside to use
the boom truck to place the cover.
·
Jason tested the remaining gauges, which all
proved to be accurate, so these are now ready for refitting.
·
Jane finished stripping the air tanks. These are now ready for painting.
·
With Jim West's assistance we refilled the milk
car so should now have a water supply sufficient to support testing under
pressure. We have now run about 9000
gallons of water thru the boiler which should have removed most of the debris
from sand blasting. From now on we
should be able to re-circulate the water.
In other areas:
·
Stu and Bob ran the wiring for the planer. The one remaining requirement is to locate a
breaker to fit our old style supply panel.
·
Dennis was rebuilding the damaged grease keeps
for the axle boxes on #428.
So a lot was achieved this week. Hopefully next weekend we should be able to
fit the inspection hatch and start testing under pressure.
Nigel
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...