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Sunday, August 25. 2013
Steam Department Update 08-24-2013 Posted by Nigel Bennett
in Steam Department at
21:49
Comments (16) Steam Department Update 08-24-2013It was a week of very hard work leading to a huge milestone. As described last week, we had reached the frustrating point of chasing leaks around the tube ends and a small check list of other minor issues requiring correction in order to get the boiler fit for the formal hydro test. Brian Davies is staying at Union for three weeks to help with the work and he put in long hours with some of us who were able to spend a day at Union during the week. Several important tasks were achieved. With Jason, he was able to largely complete the cleaning and checking of the air brake valves. However the key focus was the boiler. As the number of leaking tubes decreased, they became more frustrating and more inclined to cause an adjacent tube to leak when you rolled them. The final session on Saturday had many of us involved during the day and lasted until 11 at night but by the end, we were down to one super heater flue that has a small leak around it that we expect will seal itself when the boiler is fully heated, although it drips very slowly under hydro pressure.
So, Brian, Jim and I were back in the shop at 8:30 on Sunday, unfortunately not to assist with the last day of Thomas but to meet with the FRA inspector for the formal hydro test. I am glad to say that the old lady passed !. Aside from the tube end and a few drips from tri-cocks and blow down valves she held pressure very well with no sign of leakage. So Saturday was rather a frustrating day. Very little on 1630, aside from the tubes, could be worked on until the hydro was completed. Cameron and Phil worked with Tom on the bolster for the Shay.
Richard and Ed continued to work on preparing the cladding for lagging in the cab. Bob finally received a suitable breaker to link the planer into the supply panel. So he was able to continue work on running power to the planer. However on Sunday, after the test, a great deal of work opened up. The tubes can now be beaded so, in preparation for that, I spent quite a while in the smokebox grinding tube ends to the exact 1/4 inch required to form good bead. Later Brian took over and, by the time that I left, we were close to the point where he can bead all flues and tubes in the smokebox that are to be beaded. Ideally we want to get this done in the next couple of days so that the beaded tubes can be tested for leaks by Wednesday. On Wednesday we hope to take off the dome cover, drain the boiler and start drying it out so that the inspector can carry out the internal inspection on Friday. This is a Federal requirement. When a boiler has been over pressured, as it is for the formal hydro test, it must be inspected to ensure that nothing internal, such as the brace attachments, has been damaged or loosened. After this, any pressure testing is strictly limited to boiler pressure (180 psi). If any pressure beyond this is applied a further internal inspection is required. Beading of the smokebox end is essential before a lot of work starting with refitting the super heater elements and then moving on to the rest of the smokebox equipment can be undertaken. In the cab, work will now start on lagging the firebox and fitting the cladding so that all the controls can be finally refitted. With the hydro complete, we can now start covering the boiler again. Up until today, none of this could be started as a clear view of all the surfaces of the boiler was required for the inspection. In the firebox, Jerry applied the protective paint to the patch and rivets below where the grates will fit. Once this is dry, the grates that have been removed while we worked on the patch, will be refitted. One key thing about the milestone today is that, while she may currently look less complete than she did in 2011, we have actually passed the key inspection step for which we were preparing in Spring 2011 when we hit the problem with the firebox. So overall a very successful week. While not too much visible has changed, but we have removed the barrier to a whole lot of tasks that will make 1630 look much more like an operating locomotive again in the next month. Nigel Tuesday, August 20. 2013Steam Department Update 08-17-2013
A lot of work, a good deal of progress and some frustration. That is probably a good summary of the week in the steam shop. While a few of the team were able to assist with Thomas, most of us were hard at work in the shop.
Everything is focused on getting the hydro test for 1630 completed.
Tom, Mike and a small team worked long hours on Wednesday to get the two stays installed. They were in place ready for the Saturday team. Brian Davis and Jason, inside the firebox, worked with Brian and Sean, on the bucker in the cab, to hammer over the ends inside the firebox to compete the installation. This was a rotten job as the stays are high up above the arch tubes on the back sheet of the firebox. This makes it a very awkward place to operate the air hammer. However, they did it and the stays proved leak free in all the subsequent testing.
Life was no easier for the team in the firebox because we need to have the water in the boiler heated to 100 - 105 F and this takes a while for the pool heater to achieve. So, while they worked in the box, we had increasingly warm water circulating around it (not up to the level of the two stays but well up the sides of the box). So, by working inside a hot water radiator we were able to ensure that none of us who worked on the firebox tube ends during the day were in any danger of suffering from the cold on an 80 degree day !!.
By lunchtime we were able to apply pressure to the boiler. The more significant leaks from three weeks ago were corrected so there was now no problem with getting to the full pressure required for the hydro (1.25 times operating pressure so 225 psi). Various leaks were found and corrected. This is an iterative process, test, identify, tighten and retest. At one stage on Saturday we did think that we might be able to do the formal hydro on Sunday. However tiny leaks around tube ends proved frustratingly difficult to close. This is one of the joys of working with a steam locomotive boiler. Since the tube sheet consists of many holes close together, the force of expanding one tube can easily cause a minor movement to the next tube so you can spend a good deal of time chasing tiny leaks from one tube to the next before you get everything tight. I went back on Sunday morning to work with Brian, who is staying at Union for 3 weeks or so, and we still further reduced the number of leaking tube ends. However, it will be a continuing process during the week and probably into next weekend to get all the tube ends completely tight.
The pictures look extremely dull but are all the better for that. The tiny leaks can be seen around tube ends in the smokebox.
The overall rate of leakage is very gratifying. This small area is now the most significant
group of tube ends to be tightened. You
have to look closely in the center to see the small seepage that we must stop.
The real achievement is not apparent at the smokebox end. The sheet and tubes are actually under 225 psi pressure when you look at the gauge in the cab!!.
The new stays are
leak free at 225 psi.
The pressure drops from 225 at barely 1 psi per minute, an indication that the leaks are tiny in volume. However, where they are in areas like the tube ends, they must be completely corrected. So a week of frustrating work, tightening groups of tube ends and then checking the results with another pressure test lies ahead. If we get too frustrated, it is good to think back to the fact that, not long ago, the boiler was wide open. Now we can routinely plan to leave it totally full with minimal leakage for days on end.
The one unexpected item discovered was the union nut at the bottom of the fireman's gauge glass. Tiny droplets of water appearing thru what should be solid brass were an indication of hairline cracking. Tom now had quite a few hours of work to produce a replacement for the hydro test but I understand that this was fitted on Sunday afternoon.
Updates from Brian so far indicate that most of the leaks have been corrected by Tuesday so we hope that we can move on to other work next weekend around the planned hydro test on Sunday.
Nigel
Sunday, August 11. 2013
Steam Department Update 08-10-2013 Posted by Nigel Bennett
in Steam Department at
11:03
Comments (0) Steam Department Update 08-10-2013
There has been a lot of progress in the steam shop in the
last two weeks. The team was hard at
work last weekend while I was relaxing in the UK (and having an interesting
visit to the Great Central Railway). A
lot more was done during the week and this weekend, but unfortunately we have
seen the date when we expect to be ready for the formal hydro test drop back a
week.
The reason for the delay is frustratingly simple. As reported two weeks back, the unexpected issue found in the first pressure testing was leakage from the sockets of two flexible stays. This necessitated the removal and replacement of the stays and their sockets. While we have some spares on it site, it turned out that we had in stock only one suitable blank, from which to make the new stays. Tom managed to locate a source that could supply more from stock but these only arrived this week. (The available from stock is rather critical as they can be made but the lead time for this is 6 weeks plus !).
So the second of the stays is still being machined and ................. it is sort of difficult to pressure the boiler to test all the other defect correction when you have a 1 inch hole in it where the stay should be !.
During the last two weeks a lot has been done on 1630:
· Over the last two Saturdays all the tube ends, that were identified as having leakage, have been re-rolled. This included both super heater and small tubes at both ends.
· The old stay sockets were ground flush and removed from the backhead .
· On Thursday evening Dennis welded the new stay sockets into the backhead. This requires that the socket be accurately positioned using a special tool seen below. The socket is positioned on the tapered holder and the tapered thread is then screwed into the hole in the inner firebox.
The end can then be
slid along the shaft until the socket is tight against the backhead. It is held by the rod in the correct
orientation to align exactly as the stay will do.
Held in this way the socket can be tack welded into place. The tool is then removed and the socket welded into place.
The purpose of the weld is not to hold the socket against pressure (the stay and the fact that the socket is far larger than the hole in the backhead will do that) but to ensure that the seal to the backhead is steam tight.
By the end of the evening both sockets were in place and ready for their new stays.
· Dennis also made good a small area of the caulking between the inner firebox sheet and the mud ring that had shown some seepage under pressure;
· Mike, Jim and Jerry used the special taps to enlarge and thread the stay holes in the inner firebox sheet ready to receive the new stays, while Mike prepared the copper rings that seal the cap into the socket.
· Aside from investing a lot of time locating the spares, Tom has been machining the replacement stays. One is now threaded and just about ready to fit while the other is getting under way. A significant amount of work is required to turn each blank into a stay ready for fitting. This shows a blank alongside one of the old stays.
Each one requires:
o Slotting the head of the ball (to allow the stay to be screwed into the firebox);
o Polishing any ridges off the ball;
o Drilling the tell tale hole along the length of the stay;
o Reducing the diameter to the exact size required for threading. (Each time that a stay is replaced the size is increased by 1/32nd as the new thread is cut into the inner firebox). Just to ensure life is not simple, the two being replaced prove to be marginally different in size.
o Finally cutting the thread on the stay.
o Only once this is done can the stay be screwed into the firebox and hammered over. After all the preparatory work, the final fitting is relatively quick.
o The current plan is that the machining and fitting will be done Sunday and during the coming week.
· The fireman's side water gauge was removed and refitted to correct a leak detected under pressure;
· The engineer's side water glass was fitted so that it can be part of the next pressure test;
· The unions to both check valves were split and remade. It was found that the copper sealing ring on the engineer's side was missing. This could explain why this was leaking under pressure. A new ring was annealed and the union remade so we believe that this should be much improved.
· With all the defects that were noted under pressure corrected, but being unable to test this work, we moved on to other tasks:
o Jason worked on examination and cleaning of the air brake valves;
o Mike and Phil started preparing the air compressor for operation. The valves in the compressor all need to be opened, cleaned, lapped where necessary, and lubricated so that it is ready for testing as part of the steam test. Once the cleaning is done we will plan to test it initially using compressed air;
o The cab was cleaned up and the first major group of back head fittings was reinstalled. This includes the flange and hydrostatic lubricators. These were fitted first as they are needed to allow the air pump supply line to be pressurized. It is good to see the cab starting to take shape again !.
So, in the next week, everything rests on the progress of Tom and the team can make in machining and fitting the stays. If they can complete this during the week, we will plan to test the tightness of the boiler and fittings again next weekend.
Nigel
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