There has been a lot of progress in the steam shop in the
last two weeks. The team was hard at
work last weekend while I was relaxing in the UK (and having an interesting
visit to the Great Central Railway). A
lot more was done during the week and this weekend, but unfortunately we have
seen the date when we expect to be ready for the formal hydro test drop back a
week.
The reason for the delay is frustratingly simple. As reported two weeks back, the unexpected
issue found in the first pressure testing was leakage from the sockets of two
flexible stays. This necessitated the
removal and replacement of the stays and their sockets. While we have some spares on it site, it turned
out that we had in stock only one suitable blank, from which to make the new
stays. Tom managed to locate a source
that could supply more from stock but these only arrived this week. (The available from stock is rather critical
as they can be made but the lead time for this is 6 weeks plus !).
So the second of the stays is still being machined and
................. it is sort of difficult to pressure the boiler to test all
the other defect correction when you have a 1 inch hole in it where the stay
should be !.
During the last two weeks a lot has been done on 1630:
·
Over the last two Saturdays all the tube ends,
that were identified as having leakage, have been re-rolled. This included both super heater and small
tubes at both ends.
·
The old stay sockets were ground flush and
removed from the backhead .
·
On Thursday evening Dennis welded the new stay
sockets into the backhead. This requires
that the socket be accurately positioned using a special tool seen below. The socket is positioned on the tapered
holder and the tapered thread is then screwed into the hole in the inner
firebox.
The end can then be
slid along the shaft until the socket is tight against the backhead. It is held by the rod in the correct
orientation to align exactly as the stay will do.
Held in this way the socket can be tack welded into
place. The tool is then removed and the
socket welded into place.
The purpose of the weld is not to hold the socket against
pressure (the stay and the fact that the socket is far larger than the hole in
the backhead will do that) but to ensure that the seal to the backhead is steam
tight.
By the end of the evening both sockets were in place and
ready for their new stays.
·
Dennis also made good a small area of the
caulking between the inner firebox sheet and the mud ring that had shown some
seepage under pressure;
·
Mike, Jim and Jerry used the special taps to enlarge
and thread the stay holes in the inner firebox sheet ready to receive the new
stays, while Mike prepared the copper rings that seal the cap into the socket.
·
Aside from investing a lot of time locating the
spares, Tom has been machining the replacement stays. One is now threaded and just about ready to
fit while the other is getting under way.
A significant amount of work is required to turn each blank into a stay
ready for fitting. This shows a blank
alongside one of the old stays.
Each one requires:
o
Slotting the head of the ball (to allow the stay
to be screwed into the firebox);
o
Polishing any ridges off the ball;
o
Drilling the tell tale hole along the length of
the stay;
o
Reducing the diameter to the exact size required
for threading. (Each time that a stay is
replaced the size is increased by 1/32nd as the new thread is cut into the
inner firebox). Just to ensure life is
not simple, the two being replaced prove to be marginally different in size.
o
Finally cutting the thread on the stay.
o
Only once this is done can the stay be screwed
into the firebox and hammered over.
After all the preparatory work, the final fitting is relatively quick.
o
The current plan is that the machining and
fitting will be done Sunday and during the coming week.
·
The fireman's side water gauge was removed and
refitted to correct a leak detected under pressure;
·
The engineer's side water glass was fitted so
that it can be part of the next pressure test;
·
The unions to both check valves were split and
remade. It was found that the copper sealing
ring on the engineer's side was missing.
This could explain why this was leaking under pressure. A new ring was annealed and the union remade
so we believe that this should be much improved.
·
With all the defects that were noted under
pressure corrected, but being unable to test this work, we moved on to other
tasks:
o
Jason worked on examination and cleaning of the
air brake valves;
o
Mike and Phil started preparing the air
compressor for operation. The valves in
the compressor all need to be opened, cleaned, lapped where necessary, and
lubricated so that it is ready for testing as part of the steam test. Once the cleaning is done we will plan to
test it initially using compressed air;
o
The cab was cleaned up and the first major group
of back head fittings was reinstalled.
This includes the flange and hydrostatic lubricators. These were fitted first as they are needed to
allow the air pump supply line to be pressurized. It is good to see the cab starting to take
shape again !.
So, in the next week, everything rests on the progress of Tom
and the team can make in machining and fitting the stays. If they can complete this during the week, we
will plan to test the tightness of the boiler and fittings again next weekend.
Nigel