Sunday, July 14. 2013
Steam Department Update 07-13-2013 Posted by Nigel Bennett
in Steam Department at
11:13
Comments (7) Steam Department Update 07-13-2013A busy day with some big ups and downs in the steam shop. There is not much to see externally and only one photograph this week but this shows a big milestone. We put water into the boiler for the first time. The focus was on 1630 and above all on starting to test the newly fitted tubes for leaks. · In the morning the focus was on closing every hole below the crown sheet level: the last remaining wash out plugs were installed, lubricated with graphite paste and tightened down; the pressure gauges were finally fitted and plumbed in to the boiler; all remaining flexible stay caps were cleaned, lubricated with graphite paste and tightened down. · Just after lunchtime this was done. We linked up the hoses from the milk car and started pumping. To be clear, there is no intention to pressurize at this point. We need to fill and empty the boiler several times before we can apply pressure. Pressure testing is carried out with water heated to about 100 degrees by circulating thru the pool heater. It is rather important that we wash out debris such as residual sand blast material before trying to re-circulate the water thru the pump !. These filling and draining cycles also allow initial testing of the sealing the tubes and other parts of the boiler. While no external pressure is applied, the boiler is at least 6 feet to the crown sheet so there is a good deal of pressure simply from the depth of water. The first filling was rather disappointing for those of us who had not seen this done before. I had expected some leakage from the tubes, where they seal into the sheets, when water was first added but had probably not expected leakage from 30 or more of the small tubes, some of it quite extensive. On closer review, it indicated some variation in how much we had expanded the tubes at different times. Interesting, we were not conscious on any great difference as we did the expansion but the water was very revealing. The smokebox was excellent. There are no more than 4 tubes there that show any leakage and then no more than a dribble. Great job by Brian, who did most of this area. In the firebox, the engineer's side was relatively good while the lower fireman's side had a substantial number of tubes with a lot of leakage. Clearly we did not get these as tight as other areas. So we noted the leaks, dumped the water, which came out looking really dirty, and got working. Brian and others set up the air motor driven expander and worked thru the list of 30 or so small tubes that had been noted with leaks. At the same time, others worked on a few issues noted such as a weeping plug, a couple of stay caps that had been missed and a check valve that was not fully closed. A second filling in early evening was very satisfying. Although there was still a lot of leakage from super heater flues - no surprise as we had not worked these, the improvement in the small tubes was remarkable. We still had around 8 with minor dribbles but these were generally ones we had not previously noted, probably because the leakage was missed at the first pass due to the far greater leakage from other tubes. All those that had been worked on after the first test were dry. In addition the minor leaks other than at tube ends were all now dry.
The shot above may look a bit confusing but is a big milestone for us. Water now covers all the tubes. Compare this to shots 6 months ago, when this area was wide open and you could look down on the open holes in the firebox tube sheet. It also shows the patches of debris lifting off the crown sheet as the water starts to cover it. This is the last area from which we must wash the debris before we can circulate the water thru the pump and heater to carry out pressure testing. The water was dumped again. This time it did not look significantly different from the input water. We will need to make sure that have thoroughly washed any debris off the top of the firebox crown but it looks as if we are now close to the point that the boiler is clean enough to allow us to circulate the water. Mike and I worked into the evening hand rolling the first of the super heater flues that were flagged as leaking. Hopefully we can get the same "night and day" result on these that we achieved with the small tubes. · While we worked on the water filling and tube ends, Mike, Tom and Jerry had been working on the blanking plate for the dry pipe. The throttle is now blanked off and ready for pressure testing. · Richard, Rick and others worked on the studs and nuts for the inspection hatch and dome cover. These are now clean and the threads prepared ready to fit these covers. Hopefully in the next week we can have the tube ends sealed tight under water pressure and the hatches in place so that we can move to the next step of applying some pressure. · Jane did a great job stripping the air tanks. These are now nearly ready to prime and repaint. This is a very unpleasant job involving long stints of needle chipping and wire brushing which creates nasty black dust. Anyway, nearly done. · Stu checked out and regenerated the softener in the water supply box car. This confirms that we have a full supply of clean water to keep on with the testing . Now all we need to do is get the diesels off the end of the steam shop spur so that we can move the water car to and from the supply water supply!!. While almost the whole team was busy on 1630, Bob and Stu have been working steadily on the wiring for the planer. Much of the conduit is now in place and we are moving toward the point when we will be able to start testing the operation. So it was a pretty successful day and we look forward to further testing next week. Nigel Sunday, July 7. 2013
Steam Department Update 07-06-2013 Posted by Nigel Bennett
in Steam Department at
19:23
Comments (9) Steam Department Update 07-06-2013
A brief update courtesy of Phil as I was not at the steam shop this weekend.
On 1630 a major milestone is achieved. The firebox corner that was the cause of her withdrawl from service is now completely restored.
· The stays were fully fitted, cut to length and then formed with the air hammer. They can now be seen fully fitted into the patch and ready for service;
· Jason instructed Collin, Phil and others in the use of the gauge testing equipment. The boiler pressure gauges were successfully tested and can now be finally fitted in the cab;
· Phil and Jerry carried out a tricky "fishing exercise" and managed to extract two ferrules that had dropped into the bottom of the boiler barrel during tube fitting. Not absolutely essential but a great deal better that they are not loose in the bottom of the boiler;
· Work is progressing on refitting the remaining flexible stay caps were loose following removal for inspection and cleaning of the stays;
· Brian, Paul and David made good progress on stripping the air tanks.
Meanwhile Bob is starting to install the ducting to provide a permanent power supply to the planer.
.............. and lastly a reminder. IF YOU DO NOT ALREADY HAVE YOUR TICKETS FOR THE STEAM DEPARTMENT BENEFIT next Sunday (14th) at the San Filippo Estate- THERE ARE STILL A FEW AVAILABLE. They can be booked from the link the IRM website. Hope to see you there.
Nigel
Friday, July 5. 2013
Steam Department Update 07-03-2013 Posted by Nigel Bennett
in Steam Department at
09:37
Comments (0) Steam Department Update 07-03-2013An interim update this week as I was at the shop on Wednesday with my son who is visiting from the UK. With additional work sessions Sunday and Wednesday a lot was achieved. On 1630 the primary focus is on the remaining tasks to get the boiler water tight for initial testing. · Phil has now finished caulking the rivets inside the firebox so the rivets are now complete subject to hydro testing; · The major remaining task is fitting the two new flexible stays into the patch. These are steel rods with domed heads that must be threaded into the inner firebox and tightened so that the domed head makes a seal with the socket in the outer firebox. Here
you can see the holes in the inner firebox into which the stays will be
screwed. The end of the thread cutter is
projecting from the right hand hole.
Viewed
from the outside we can see the two sockets.
The one on the right is empty and, thru the socket, you can see the hole
in the inner firebox into which the thread will be cut. The guide and cutter are in place in the left
hand socket ready to start cutting.
Here
Tom is setting up one of the stays to cut the thread on the stay itself.
Here
the thread is being cut. This also gives
a good view of the overall shape of the stay with the thread being cut at one
end and the ball, nearest to the camera, which will seat into the socket. The slot in the ball is essential to allow
the stay to be screwed into the threads in the inner firebox.
Here
Michael is manually cutting the thread into the inner firebox sheet. Good progress was made and by evening the stays were being screwed into place. This is not a "one-time" operation as the threads must be carefully adjusted so that they are tight but not excessively so in the threads of the inner firebox when firmly in contact with the socket. Once this is achieved the inner end is to be peaned over and caulked to complete the sealing Another major task completed Wednesday was the hammer and hydro-testing of the three air tanks. All were successfully tested to 180 psi and have now been partially stripped of paint. Paint stripping will continue so that they can be repainted before fitting. A lot of preparatory work was required for the hydro-testing, which has commissioned and tested the equipment needed for the boiler testing in the next few weeks. The water for testing both tanks and boiler must be warm. The heating is achieved by circulating thru a pool heater. Preparing the pump and heater system for use after winterization requires several hours work. This was successfully achieved and the system is now tested and ready for use in the boiler testing. I will not be at Union this Saturday so will look forward to an update myself on Sunday ! Nigel |
Blog AdministrationCategory TreeCalendarQuicksearchSyndicate This Blog |
Powered by s9y.
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]