Monday, August 12. 2013Wood Shop Update - August 10-11, 2013Here is an action shot of a new band saw blade uncoiling itself after being tossed out of harm's way. I bet we could script a lame tv show for this type activity. And if you did not get hurt - you might advance to the next round where you could fold it up again into three coils. Here, Tim Peters is safe and sound. This is a new heavy duty resaw blade that Tim will use to cut massive timbers for new end sills for Chicago Rapid Transit 1024. It is hard to shoot a pic upward into a clear sky, but that is Bill Peterson finishing off removal of old paint on the front roof of Chicago Great Western X 38, our Russell Plow. Victor Humphreys is applying the maroon finish paint to the primed north side of the plow. It makes a huge difference, but remember, we will apply a second coat. I find it interesting that the code string for this image came up "CIA" but do not know what that means, or if we are in trouble with the government. Buzz Morisette is working to let in new mortises for hinges to allow a last new door to be hung on the north side of the plow. For now it remains unhinged. Every day we try to make some more progress on the the parts of the plow remaining painted in the ever popular 'rust' and 'yellow' colors. Soon all traces of the C&NW yellow will be gone. Victor is ready to prime more of the ramp, while Bill Peterson and Paul Cronin stand by. They largely did the paint removal. Randall Hicks is taking a break and is sitting on the replacement compressor for Chicago Aurora & Elgin 36 wood interurban. They hooked up a 600 volt stinger cable to it and ran it for a while to check it out and it passed the test. If something unexpected comes up and this is not needed, I think this would make a stylish and chic conversation piece in the living room. Bill Wulfert is removing paint (many layers) from some 'pie pan' light shades. They are destined for the 50th Avenue high level platform lighting. Bob Sundelin is routing new carlines using a template and pattern routing bit. These are to be installed as part of an all new set in Union Pacific M 35. Sunday, August 11. 2013
Steam Department Update 08-10-2013 Posted by Nigel Bennett
in Steam Department at
11:03
Comments (0) Steam Department Update 08-10-2013
There has been a lot of progress in the steam shop in the
last two weeks. The team was hard at
work last weekend while I was relaxing in the UK (and having an interesting
visit to the Great Central Railway). A
lot more was done during the week and this weekend, but unfortunately we have
seen the date when we expect to be ready for the formal hydro test drop back a
week.
The reason for the delay is frustratingly simple. As reported two weeks back, the unexpected issue found in the first pressure testing was leakage from the sockets of two flexible stays. This necessitated the removal and replacement of the stays and their sockets. While we have some spares on it site, it turned out that we had in stock only one suitable blank, from which to make the new stays. Tom managed to locate a source that could supply more from stock but these only arrived this week. (The available from stock is rather critical as they can be made but the lead time for this is 6 weeks plus !).
So the second of the stays is still being machined and ................. it is sort of difficult to pressure the boiler to test all the other defect correction when you have a 1 inch hole in it where the stay should be !.
During the last two weeks a lot has been done on 1630:
· Over the last two Saturdays all the tube ends, that were identified as having leakage, have been re-rolled. This included both super heater and small tubes at both ends.
· The old stay sockets were ground flush and removed from the backhead .
· On Thursday evening Dennis welded the new stay sockets into the backhead. This requires that the socket be accurately positioned using a special tool seen below. The socket is positioned on the tapered holder and the tapered thread is then screwed into the hole in the inner firebox.
The end can then be
slid along the shaft until the socket is tight against the backhead. It is held by the rod in the correct
orientation to align exactly as the stay will do.
Held in this way the socket can be tack welded into place. The tool is then removed and the socket welded into place.
The purpose of the weld is not to hold the socket against pressure (the stay and the fact that the socket is far larger than the hole in the backhead will do that) but to ensure that the seal to the backhead is steam tight.
By the end of the evening both sockets were in place and ready for their new stays.
· Dennis also made good a small area of the caulking between the inner firebox sheet and the mud ring that had shown some seepage under pressure;
· Mike, Jim and Jerry used the special taps to enlarge and thread the stay holes in the inner firebox sheet ready to receive the new stays, while Mike prepared the copper rings that seal the cap into the socket.
· Aside from investing a lot of time locating the spares, Tom has been machining the replacement stays. One is now threaded and just about ready to fit while the other is getting under way. A significant amount of work is required to turn each blank into a stay ready for fitting. This shows a blank alongside one of the old stays.
Each one requires:
o Slotting the head of the ball (to allow the stay to be screwed into the firebox);
o Polishing any ridges off the ball;
o Drilling the tell tale hole along the length of the stay;
o Reducing the diameter to the exact size required for threading. (Each time that a stay is replaced the size is increased by 1/32nd as the new thread is cut into the inner firebox). Just to ensure life is not simple, the two being replaced prove to be marginally different in size.
o Finally cutting the thread on the stay.
o Only once this is done can the stay be screwed into the firebox and hammered over. After all the preparatory work, the final fitting is relatively quick.
o The current plan is that the machining and fitting will be done Sunday and during the coming week.
· The fireman's side water gauge was removed and refitted to correct a leak detected under pressure;
· The engineer's side water glass was fitted so that it can be part of the next pressure test;
· The unions to both check valves were split and remade. It was found that the copper sealing ring on the engineer's side was missing. This could explain why this was leaking under pressure. A new ring was annealed and the union remade so we believe that this should be much improved.
· With all the defects that were noted under pressure corrected, but being unable to test this work, we moved on to other tasks:
o Jason worked on examination and cleaning of the air brake valves;
o Mike and Phil started preparing the air compressor for operation. The valves in the compressor all need to be opened, cleaned, lapped where necessary, and lubricated so that it is ready for testing as part of the steam test. Once the cleaning is done we will plan to test it initially using compressed air;
o The cab was cleaned up and the first major group of back head fittings was reinstalled. This includes the flange and hydrostatic lubricators. These were fitted first as they are needed to allow the air pump supply line to be pressurized. It is good to see the cab starting to take shape again !.
So, in the next week, everything rests on the progress of Tom and the team can make in machining and fitting the stays. If they can complete this during the week, we will plan to test the tightness of the boiler and fittings again next weekend.
Nigel
Friday, August 9. 2013YouTube Channel, IRMTVOnline.We now have a YouTube channel, IRMTVOnline!. I want to thank Nick Espevik for a great job on editing this video. Here is the link: http://www.youtube.com/watch?v=G5PLp3GDLPk |
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Comments
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