A lot of work, a good deal of progress and some
frustration. That is probably a good
summary of the week in the steam shop.
While a few of the team were able to assist with Thomas, most of us were
hard at work in the shop.
Everything is focused on getting the hydro test for 1630
completed.
Tom, Mike and a small team worked long hours on Wednesday to
get the two stays installed. They were
in place ready for the Saturday team.
Brian Davis and Jason, inside the firebox, worked with Brian and Sean,
on the bucker in the cab, to hammer over the ends inside the firebox to compete
the installation. This was a rotten job
as the stays are high up above the arch tubes on the back sheet of the
firebox. This makes it a very awkward
place to operate the air hammer.
However, they did it and the stays proved leak free in all the
subsequent testing.
Life was no easier for the team in the firebox because we
need to have the water in the boiler heated to 100 - 105 F and this takes a
while for the pool heater to achieve. So,
while they worked in the box, we had increasingly warm water circulating around
it (not up to the level of the two stays but well up the sides of the box). So, by working inside a hot water radiator we
were able to ensure that none of us who worked on the firebox tube ends during
the day were in any danger of suffering from the cold on an 80 degree day !!.
By lunchtime we were able to apply pressure to the
boiler. The more significant leaks from
three weeks ago were corrected so there was now no problem with getting to the
full pressure required for the hydro (1.25 times operating pressure so 225
psi). Various leaks were found and
corrected. This is an iterative process,
test, identify, tighten and retest. At
one stage on Saturday we did think that we might be able to do the formal hydro
on Sunday. However tiny leaks around
tube ends proved frustratingly difficult to close. This is one of the joys of working with a
steam locomotive boiler. Since the tube
sheet consists of many holes close together, the force of expanding one tube
can easily cause a minor movement to the next tube so you can spend a good deal
of time chasing tiny leaks from one tube to the next before you get everything
tight. I went back on Sunday morning to
work with Brian, who is staying at Union for 3 weeks or so, and we still further
reduced the number of leaking tube ends.
However, it will be a continuing process during the week and probably
into next weekend to get all the tube ends completely tight.
The pictures look extremely dull but are all the better for
that. The tiny leaks can be seen around
tube ends in the smokebox.
The overall rate of leakage is very gratifying. This small area is now the most significant
group of tube ends to be tightened. You
have to look closely in the center to see the small seepage that we must stop.
The real achievement is not apparent at the smokebox
end. The sheet and tubes are actually
under 225 psi pressure when you look at the gauge in the cab!!.
The new stays are
leak free at 225 psi.
The pressure drops from 225 at barely 1 psi per minute, an
indication that the leaks are tiny in volume.
However, where they are in areas like the tube ends, they must be
completely corrected. So a week of
frustrating work, tightening groups of tube ends and then checking the results
with another pressure test lies ahead.
If we get too frustrated, it is good to think back to the fact that, not
long ago, the boiler was wide open. Now
we can routinely plan to leave it totally full with minimal leakage for days on
end.
The one unexpected item discovered was the union nut at the
bottom of the fireman's gauge glass.
Tiny droplets of water appearing thru what should be solid brass were an
indication of hairline cracking. Tom now
had quite a few hours of work to produce a replacement for the hydro test but I
understand that this was fitted on Sunday afternoon.
Updates from Brian so far indicate that most of the leaks
have been corrected by Tuesday so we hope that we can move on to other work
next weekend around the planned hydro test on Sunday.
Nigel
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]