Tuesday, February 2. 2010Track Dept Weekend Report
Toms report from Saturday and my report from Sunday-
Saturday- Yesterday Frank and I got there so that we could help with the Electric Car folks with the first moves into Barn 11 - as no one was about in the morning, we dug into the list of stuff to do in Barn 2 - starting with the starter of course. As I noted below - Frank dug out that one from the 585, we did the switch with the 580 and got the 585 running. We let it run a while to warm up and starter in on the 6000. We changed out the broken pin on the right work head, and on the good advice of Frank decided to change the left one too since I bought two new pins... good thing as that one was broken too, hanging on but less the a 1/4 inch...yikes... So it goes to show - inspect your machine as much as you can... Both are now new. After all that was done, Adam showed for the 2nd trick. We headed to Yard 11, to wake up the 50. It took a while with the normal trans oil and warm up, we had to thaw out the transmission air lines too - but it fired up fairly well for having sat for a month... In the end it was not needed - so that ended a good day (Seems the EJ&E folks installed the wrong starter in the 585 - one with too small teeth on its gear - that DID grind away some on the fly wheel, but after Frank removed the 585 starter and we went into the barn to see what was on the 580 (how cool to have spare motor cars huh?) and saw it was a lot bigger motor on the 580... sooo..switcho we did -) Tom Hunter -------------- Sunday- Tom and I made up the gang and chose to clean off the CNW flatcar of 'stuff' gathered from along the RoW with the Burro crane we serviced Saturday. Tom fired up the Model 50 in Yard 11 and I went to retrieve wreck knuckes and such. The CNW flat was buried in the middle of a string of cars on Station Tk 2 so we had to move a bunch of cars to get it out. I do believe the Model 50 moved more tonnage that day than ever before! We moved a very heavy six axle flat, eight axle flat and Rock Island coach uphill in one pull! With a full transmission and full throttle it crept the cars upto the main at a brisk 1-2MPH... It was amazing. After making the switch we headed to yard 14 to unload a slew of line poles we had picked up from Schmidt Siding and then went to the diamond at South Jct to unload three old signal foundations from the old 151/ 152 signals. Tom reported how heavy the things were to pick up. 6000lbs is not light. We finished the heavy lifts and ran the flat back to station 2 and put away all of the other cars. We tied up the crane and called it a day. I bought three sheets of 3/4" plywood for a little shelf project in Tk24. I hope to start that soon. On another note it, the diesel guys plan on switching the shop on Track 24... That means we'll have to clear out ALL of the track machines from the Barn. Included is the old brush cutter in the heated portion of the shop. If anyone is working on it, please let me know as it may be moved permanently out of the shop due to track space issues. Take Care, Adam Robillard IRM Track Dept Tuesday, November 17. 2009
Track Dept Weekend Report - November ... Posted by Adam Robillard
in Track Department at
18:38
Comments (0) Track Dept Weekend Report - November 14/15
Saturday's gang began with Greg Frech, JD Marzec and Adam Robillard.
We received 100tons of ballast this past week and it was time once
again to load ballast cars and continue working on surfacing yard 11
(outside of the barn) as well as the tail track lead at the Yard 13
diamond. Greg and JD were on the Model 50 Burro crane crew and sorted
material throughout the yard. We had lots of scrap, rails, timbers,
etc scattered all over the yard and they spent all morning loading the
gondola and stacking material. In the meantime,
Adam loaded our green CNW ballast car with the Model 30 Burro crane.
Joel Ahrendt received his first lesson on the Model 30 as well and now
has a good taste at what it takes to load a ballast car. Typically
each full car takes roughly a day (8hrs) to load with the clam shell
bucket.
By lunchtime, Adam had nearly 3/4 of the ballast car full and asked to use the diesel dept switch crew to help dump ballast. Jim West and Warren Lloyd as the crew of the ComEd 15 switched Yard 11 and dumped 1/2 of the car on the tail track lead. Jim West ran the engine while Warren, JD, Greg and Adam ran the doors. Finished with that Greg, JD and Adam got out the Amtrak regulator and regulated the freshly dumped ballast in prep for tamping. Dark took hold soon after and we called it a day. Sunday's gang was made up of Steve Lewkowycz, Jim West, Joel Ahrendt, Warren Lloyd and Adam Robillard. The day's priority - Tamp and Regulate. Steve L and Adam R started the day out by checking fluids and starting up the Amtrak 6000 tamper in Yard 11. We took it to the Yard 11 tail track and set up the machine. Steve L took to the controls for his first time and made the first pass with only a minor 'cord' problem which continued to short out and trip the circuit breaker.. A quick crop of the light buggy extension cord was in order but remedied quickly. After the first pass was through we got the Amtrak regulator out and plowed stone to prep for the next pass. By this time we were joined by Jim W and Warren L who helped finish the next few passes with the tamper. Jim ran the tamper for the rest of the evening and did a fine job as this was only his second time at the controls. We made three passes on the track now it no longer resembles a roller coaster. Warren ducked out about the time Joel A showed up to help out. The next steps were to tamp 11-4 and 11-2 tracks from the Barn to the switches. We split into two gangs: Steve and Joel ran the ballast regulator while Jim and Adam ran the tamper. We did our final passes on both tracks and the crew on the regulator had them both broomed and looking like mainline track by dark! The 6000 ran great with no mechanical problems all day long.... Looks like the hard work over the past few months is paying off. Thanks to all who helped this weekend, especially Joel Ahrendt, Jim West and Warren Lloyd visiting from the other departments, as we get ready to open up Barn 11! Adam Robillard IRM Track Dept lzeje657@msn.com Wednesday, November 11. 2009Midweek Track ReportWell it turns out Veteran's Day is an Amtrak holiday... know knew? Well the weather cooperated today so I head out with a list of one man jobs to accomplish. To my surprise, JD Marzec and Greg Frech both showed up willing to do track work! Turns out they had the day off as well. So with three people the job quickly turned to Yard 11. The job was to get 11-4 track ready for another pass with the tamper so the first task was to regulate the stone that was dropped a few weeks ago. After getting the regulator fired up, Greg and JD made a few quick passes with the plow and broom. After they finished the 6000 tamper and regulator were moved to Yard 10 to clear 11-4 track. We made our way to Track 24 to fire up the tie crane and motorcar/ powerpack combo. We had to replace a ~12ft stick of rail on 11-4 track to close a 3" gap in the curve. So Greg and JD both got a walkthrough on the machines and ran them over to yard 11 while I acted as the U-man on the ground. The three of us made quick work of removing the old rail and cutting/ installing the new rail. After the last spike was through we headed for lunch at Joe's. |
Blog AdministrationCategory TreeCalendar
QuicksearchSyndicate This Blog |
Powered by s9y.
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]