Back to Union after a couple of weeks in the UK. Lots of progress in the last two weeks and a hectic day on Saturday.
The site looks very different with the snow gone and a
frenzy of activity leading up to opening day.
It is not normally this bad but the weather delays mean that work
normally done in February and March has been concentrated into just a few
weeks.
Frank and the track team, with assistance from the scouts
camping on site, were hard at work on the track of the steam lead. This has proved to be a nightmare. The section of track in front of the service
box car was very poor and was lifted in December to set new ties. Unfortunately the area was then covered by
snow and has only just re-appeared!. On
Saturday the new track was laid and we now have excellent track in the area
where we will service 1630. This
overcomes concern that, after all the work in the last couple of years, she
could have fallen thru the track in her service area. Many thanks to Frank and his team.
(Thanks to David for the above pictures)
Unfortunately this is not the end of the job. We have only recently become aware that the
big T&NO 2-10-2 (#975) rode up on the switch between the steam lead and the
car line when being moved for the Transformers filming. Substantial work is required to repair this
switch over the next few weeks and we will work with Frank’s team on this. However, we may need water for testing before
this is done and the water car was stuck in the yard behind the damaged switch. So a very careful piece of switching was done
under Frank’s supervision to pull the water cars out over the partially
repaired switch with the BrownHoist. All
went smoothly and we now have the water cars by the shop and can get water when
required.
Another interesting exercise followed!. The damage highlighted the next major
question. Why did #975 cause such damage
when moved?. She was moved at short
notice and without steam department staff present so we did not see the event. After an hour with a lot of oil and much
shunting of #975 back and forth on the “Y” with the BrownHoist we think the
problem is identified and resolved.
Absent lubrication, the bearing plates of the trailing truck were not
moving. After applying a lot of oil and
pushing slowly in and out of the curve, there was an loud bang and the truck
started moving from side to side again.
More oil and a few more trips back and forth into the curve and she
slides smoothly from side to side. A big
2-10-2 will never be happy on the curves around our site … but if lack of lubrication before movement
turns it into a 2-12-0 !!!.
(Oh well. I have just heard from Jamie that we investigated the wrong locomotive. It was #2707 not #975 that damaged the switch. At least #975 is now well lubricated!.)
Back in the shop the main effort was focused on preparing
1630 for spraying of the cab and boiler.
A lot of different tasks were progressing in parallel.
Jim and Rick were filling
and sanding areas of the cab side. In
the past two weeks, Dennis has done a lot of weld repairs to the cab sides and
these are now being finally prepared for spraying. While I was away, the decision was taken to
remove and repaint the lettering, as it was proving too difficult to preserve
the existing letters. So the cab sides are now completely stripped and stencils
are being prepared.
Eric and many others
worked on sanding down and masking the superstructure of the locomotive. The smokebox is now sheeted to protect it
from over spray. All brass pipes and
fittings, that are not to be sprayed, have been either removed or protected.
The injector starter
valves were removed from the sides of the firebox, as these were too large and
tricky to spray around.
The cab front windows are
masked. Now we are ready for the painter
to review readiness to actually do the spraying.
Jason, Collin and others
worked on the smokebox front. Some leaks
were detected in this during the November test runs. We had considered removing the front sheet
and fitting a thicker gasket. However,
the team identified that the leaks were clearly identifiable to a small number
of specific areas, visible when Collin was shut in the darkness of the smoke
box and lights were held on the outside!.
These were sealed with a high temperature sealant. So this issue should now be resolved without
the need to lift off the smokebox front again.
One of the large areas
that has been completed while I was away is the top of the tender. This is not an area usually seen by the
public, but it sure looks good despite a couple of Nigel’s dusty boot prints!.
Aside from 1630 most of the effort was focused on the
switching to bring the water cars to the shop and resolve the issue with #975. However, in the shop:
Tom was working on the
adjustments to the planer. It has
actually been set up to start some work (the axle box for a leading truck). However it is not currently advancing the
cutter horizontally or vertically between cutting strokes as it should. So work is progressing to work out why this
is and how to correct it.
I worked with Collin and
Bob on the new house air compressor. We now
have most of the parts in hand for this and will plan to activated it soon.
While the trip to the UK was largely for a family visit, I
was able to fit in a couple of visits to UK railways.
At the Bluebell Railway in Sussex I was warmly welcomed by
a couple of the teams building largely new steam engines. The 84030 team are building a replica of an
extinct class of BR 2-6-2T locomotive from parts of a similar 2-6-0 while the
Atlantic team are building a replica of a 1911 LBSCR 4-4-2 using a boiler that
survived in industrial use. In the latter
project much of the rolling chassis is now complete. The new axle boxes and wheel make an
interesting comparison to our efforts with #428.
The cylinders have been fabricated and are in place on the
frames.
High quality work is obvious on the Bluebell in the wood working
as well as the locomotives. These are
shots of a superb set of late 19th century Metropolitan Railway
varnished wood coaches, the restoration of which has won awards. These have been rebuilt in recent years from
an extremely run down condition.
I subsequently visited the Severn Valley Railway for the
last day of their Spring gala with 7 or 8 locos in steam. A pause to wait the crossing with another
train gave me the chance to look closely at one of their GWR Manor class
locomotives. It really highlights how
different the layout and painting of this is when compared to our #1630. Looking in this way, there is no exposed pipework. It all runs below the sheet metal, which is
almost completely unbroken. A very different
approach when I think of all the holes that we have to adjust and fill around
the many pipes and studs on our locomotive.
There was no work at the shop on Sunday as many of us
attended the memorial for our late and sorely missed friend Bill Chyna. Many thanks to Kath and Beth for the
invitation to a very pleasant afternoon remembering the good times.
Next weekend is likely to be rather quiet as many people
will need to attend the rules training and / or test in preparation for running
this season.
Nigel