A momentous couple of
weeks!. It has looked uncertain up to
the last minute but, at 3:39 on Saturday 25th May, #1630 left Union
with its first revenue train in ten years. Many thanks to Michael for the
souvenir above, which is the train order for the first revenue run.
For the last two weeks we have
been struggling to resolve the problem of brazing the crack in the smokebox
ring and completing the mesh work in the smokebox ahead of Friday 23rd,.
which was the last day when we could carry out the inspections before the
Memorial Day weekend.
Last weekend all sorts of odd
jobs were carried out to ensure that she was ready to go provided that the ring
was completed, but all in the knowledge that, without the smokebox being completed,
we would not be going anywhere.
She was moved to allow paint to
be touched up in areas hidden by the rods as she stood in one position.
The air system was pressurized,
minor leaks corrected and the brakes tested.
This lead to some intensive work when the locomotive brake would not
operate. That proved simple at the end
of the day. A drain valve that had been
jammed for some time was cleaned and reconditioned as part of the overhaul and
no one remembered to close it!.
Unfortunately house air does not allow us to test the train brake so that
only showed a problem at the last minute!.
Wedges were adjusted and
lubrication applied all around.
A lot of time was spent cleaning
and checking every aspect to ensure everything was tight and all items of tools
and debris were removed.
On Wednesday she was moved over
to the steam lead, coaled and watered.
By this stage the timing was so tight that this was done in anticipation
but there was still no certainty that the work could be completed for steaming
on Friday. In the evening Dennis made
substantial progress in welding in the mesh screens for the spark arrestor.
Everything rested on Thursday
night / Friday morning. I gave myself “a
bit of a work out” by laying a layer of coal over the grates ready to start the
fire. That certainly demonstrated that
it is a very large and long box compared to anything I ever fired in the UK!.
Brian made a mix of linseed oil
and graphite, which is the material for “painting” the hot surfaces such as the
lower firebox and smokebox. A team spent
much of the evening applying this wherever it was needed.
By late evening, Dennis had the
mesh fully installed. The key work,
visible here, was welding the brackets for the side panels into the
smokebox. This is complete in the picture
below and all that remains to be fitted is the center section which simply
bolts between the two side pieces.
Then attention moved to the
ring. After a long period of pre-
heating, to get it to an even temperature, Dennis started the repair. The clock tells it all. It was already 11 at night!.
Four areas remained to be
brazed. Two sections running out toward
the edge and two holes in the curved section.
These were holes drilled at either end of a crack to prevent it
extending. In this view Dennis has
initially sealed the one nearest to the camera and is working on the radial
crack behind..
By 12:30 the brazing was
complete and the ring post-heated to ensure that it was at an even temperature
to minimize the risk of cracking as it cooled.
The cooling had to be slow, so most of us took a couple of hours in the
sleeping car while Jeff and others finished bolting the mesh screens into
place.
By about 3 a.m. the ring was
cool enough to work (acid test – hold your hand on it indefinitely without
pain!). Jerry then spent the next hour
grinding the surface smooth and level.
Around 4 a.m. we got to the next
stage. The ring had to be drilled for
the bolts that secure the bell and a strengthening plate, to fit behind the
ring and ensure that the load was distributed evenly in the area that had
cracked, drilled to match. The look on
my face and the large coffee says it all!
Shortly after dawn the parts
were completed and efforts moved on the fitting to the locomotive.
First the ring was carefully
lifted in to place and secured.
Once this was in place the door
was lifted and located on its hinges.
Then the bell could be
mounted. This was a critical last step
in sealing the smokebox so that the fire could be lit.
A little before 8 there was a
celebratory gathering on the footplate and I had the honor of lighting the
first fire.
From there on things moved
rapidly. It is always fascinating to
watch a steam locomotive come to life again as she warms up.
In this case the old girl gave
every sign of being impatient to get into action. Within an hour there were signs of bubbling
and within two there were the first signs of pressure.
By 10:30 she was self-supporting
with the fan removed and enough pressure to operate the blower.
The critical tests went
well. The safety valve settings were as
expected and, for the first time in 45 years, she blew off at her design
pressure of 180 psi. The air pump tested
with much more reserve than last year, whether due to the higher boiler
pressure or the cleaning of the governor over winter.
From there on things went down
hill !. The locomotive air brake worked
fine but the train brake would not apply.
After much cleaning and checking of valves it would still not work so it
was decided to make a light engine test run (using just the locomotive brake).
That was a bit less than
successful when the air pump stopped on the mainline and she barely made it
back to Union.
However, the air pump issue
proved simple. The hydrostatic
lubricator feed had clogged cutting off lubrication and, once the lubricator
was operating correctly, so did the air pump.
The train brake issue was rather
more tricky. Tom, Rod and others worked
thru the evening on this. Eventually,
around 10, it was traced to a couple of issues, the most significant of which
was a leaking connection.
So on Saturday she was prepared
for service.
Water was topped up and a little
coal added. The obvious remaining item
was corrected when the dome cover was lowered into place.
This is a significant last step indicating that she is
not planned to go back into the shop for a while. The dome fouls part of the door opener
mechanism so she cannot go into the shop with this in place.
The Saturday service runs were a
little later as we were required to make two test runs (one light engine and
one with empty stock) before running a service train. This was why we had hoped to run the previous
weekend.
However, this was achieved and,
at 3:39, #1630 pulled out with her first service train in many years. A very strange feeling to see her live and
rolling across the countryside after having been all over, inside and around
her in the shop for the past several years.
The culmination of a huge effort
by a LOT of people in the steam shop.
Well done guys and gals.
The shop looked rather empty for
a few hours until #938 was moved in. I
think I am safe in saying that is not an indication that she is now next in
line to steam!. Hopefully we can now have
a few weeks on fairly mundane tasks. The
water supply is becoming rather unreliable and is in need of work if we are to
support #1630 in regular running. Also
the service area must be moved to a new location as the construction of the
Schmidt cutoff in the next few months will mean that it cannot be outside the
water supply box car as in the past. We
will also need to monitor #1630 very closely.
She has run only a very short distance on the rebuilt rear axle boxes so
is very much “running in”. These
bearings are currently running hotter than they should but that is hopefully a
matter of keeping them well greased and letting them bed in.
And finally a blatant publicity
item while we are here! –
Don’t forget the Annual Steam
Department Benefit at Sanfilippo on June 29th this year. This is a really unique and enjoyable
afternoon and a major source of funds for the continuing activity of the steam
department so we hope to see you there.
Nigel