![]() |
![]() |
Sunday, November 22. 2015
You don't have to be mad .... but ! Posted by Nigel Bennett
in Steam Department at
19:32
Comments (8) You don't have to be mad .... but !
What a difference a few days makes in Illinois!!. In the last few weeks we have been working steadily thru the jobs needed to winterize #1630 and the support equipment while enjoying a long warm Fall. Then this weekend Winter arrived with a vengeance. Small problem, this was the weekend we had a rather critical activity scheduled!!. So, neither rain nor snow etc. (Also you don’t have to be mad to work in the steam shop but it sure helps at times.
The critical activity was the FRA observed hydro test of Shay #5 which was scheduled for Sunday. Clearly large quantities of water do not mix well with temperatures falling into single digits. However we managed.
On Friday Phil managed to fill the boiler and a reserve container in the shop before draining the bottle car that provides our supply of treated water. (Just ahead of the night when temperatures plummeted).
On Saturday I managed to get to the shop between the two bands of snow. Conditions on site were “interesting” and the work team was small.
Difficult to imagine that this was just 7 days after the shot of removing the dome cover from #1630!!. Congratulations to Chris and Jon who made it in. On the Shay the objective was to get the water circulating from the boiler thru the pool heater and then get this fired up so that boiler could be brought up to around 100F and allowed to equilibrate for the test. This was subject to some significant concern as the heater is outside and, should it not operate reliably, there would be a risk of it freezing and damaging the exchanger. Much to my relief, despite digging it out of the snow and having to shield it from further driving snow during the day, it started and ran reliably so the warm up worked well.
Actually, having been used to #1630, it is startling how much quicker #5 warms up and it seems to even the heat out much more effectively because of the relatively short barrel. In the shot above you can see the inlet from the heater feeding into the dome and the return running from the blow down back along the shop to the North.
Sunday was a very pretty day, even if it was 8F when I got back to the shop, and the team could get to the site without problems. The heater restarted without issue and the boiler was ready for testing by mid-morning when the FRA inspector was scheduled. The pressure was raised slowly to 240 psi (125% of the 190 psi at which she will operate). Jason, Phil and Collin worked with the inspector to check parts of the boiler for any sign of leakage but she proved extremely tight. One small area of a seam and the head of one stay will need minor peening but we have an acceptable pressure vessel!!.
This opens up a whole lot more work for the Winter (which is why we were so desperate to get this done before it became impossible to work with water!). The boiler can now be lagged and the various accessories and their pipework fitted. The smokebox riveting should be done soon and then the smokebox can be completed and the truck refitted.
Technically there is no reason that she should not be operational next season. The biggest barrier is MONEY!. The response to the Summer appear was disappointing ($600 plus $600 in matching). Funds for #5 are now low and her operation in 2016 is going to depend heavily on donations in the next few weeks.
So, aside from this weekend, what has been happening in the last few weeks?.
#1630
Work progressed as planned.
#5 – Shay
I am sure that Brian will provide a more detailed update however a lot of progress is apparent leading up to the test today.
#938
Phil and his team completed the Summer work by painting all the wheel and lower areas that have been stripped and primed. She looks a great deal more presentable and will hopefully be able to go under cover once the new barns come into service.
#428
With the cab now riveted, Jon has been working on painting the interior and planning the woodwork that can now be fitted.
Compressor shed
Jeff and Jerry have made huge progress on the pipe work for the new compressors. Max has set up most of the wiring. The smaller of the two compressors is linked in and workable. All the main pipe work for the large compressor, including the cooling loop has been installed. The one remaining item is the flanges to connect the large compressor to the pipework. Once these are made the whole set up should be in a state to test.
Before it can be commissioned a state inspection is required so we cannot put either into operation until the whole set up is complete.
So a busy and successful couple of weeks. Now we head into a busy Winter with the objective of completing two locomotives for next season.
Nigel
|
Blog AdministrationCategory TreeCalendar
QuicksearchArchivesSyndicate This Blog |
Powered by s9y.
Comments
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]