From this point forward I'm going to start summarizing the updates by week instead of by day like we've done in the past. That might make it easier to post a little more info with my limited time. Also, I'll be making separate blog posts for the progress on 92 starting next week.
Anyway, earlier in the week Dan and I made it out to the shop one evening to work on the 7525 and 92. While Dan focused on testing the electrical system of 92 and making a list of work that it will be needing, I crawled under the 7525's number 3 traction motor to perform some cleanup. A few weeks ago, Dan had meggered all the motors and we also knew that the number 3 had flashed and needed some work. The armature was reading .1 megohms, which is not good at all.
There were obvious signs with freshly melted bronze on the brush holders and zaps from the end of the armature to the motor case. I spent a few hours slotting the entire commutator, using a lining bar to move the loco an inch or two at a time to rotate the motor and wiped everything down that I could reach with some motor cleaner to remove any carbon tracks that might be present. Slotting is where you take a file designed to fit in between the bars of the commutator and essentially file out anything that is in the slots, copper balls from flashing, carbon, dirt, etc., anything that'll conduct from bar to bar. While cleaning and inspecting the bottom of the motor, I noticed two broken springs on the same spring pack on the back holder. Made a note that it'll have to come out to be repaired. After the cleaning and slotting, megging again brought it up to .6 megohms, better.
On Saturday morning, Erik and Nick continued sanding in the cab of 411. They spent much of the day making a huge amount of progress getting most of it ready for primer.
I worked on getting the holder out of the motor on 7525 to replace the bad springs. Little did I know I would find a hole blown in the bottom of it, which is what burned through the springs. I cleaned it up, removed and cleaned all the insulators before putting it back together and reinstalling in the motor. Megged again and not it's showing just over 1 megohms, much better. We'll give it a try this season and see how it performs.
There were a number of people working on the 92, including Dan, Laddie, Nick, Erik, Brian, Colton and myself. There was a lot of paint scraping going on inside, more work on the electrical system, and some work on the air system.
Erik and I also installed a fitting on the 7525 to make prelubing the engine far easier than what we were doing.
Thanks to all these guys for all their hard work!
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...