It was a low turnout at the Steam Department today, in part because several of the team were at Harper staffing the stand at the High Wheeler show. The weather may have deterred some and it certainly was not kind to the shop!. The ice brought down a large section of guttering and the machine shop furnace failed, which lead to some time spent investigating the gas leak.
Glenn and Mike made great progress on the super heater flues. 7 of 16 are now cut and ready for safe ending.
Sand blasting was on hold as Collin was away. Jason tried but found it difficult to work in the boiler due to the accumulation of blasting sand. This made for an unstable base on which to stand in the confined space of the barrel.
We therefore brought forward the task of clearing sand from the boiler. The technique may not look pretty but it works. The material is so dense that suction is not effective. It is not easy to sweep or push in the confined space of the boiler but pushing it to the main drain plug and setting up a chute there proved to be the most effective method.
In this way we have now removed several hundred pounds of the material from the boiler.
Several key additional pieces of equipment arrived that should allow us to move forward next week. We now have the angled tips for the sand blaster that will allow the corners of the firebox to be cleaned. A dust collector was installed that improves the extraction of dust from the boiler during sand blasting.
With the arrival of a new and more powerful vacuum, substantial progress was made in removing residual lagging material. This tends to accumulate everywhere as the material fragments as it is removed. Cleaning this up to enable inspection and refitting is one of many mundane but essential steps in the overhaul.
Mike was working on the mud ring where the patch is to be installed. This is being ground out in preparation for welding to make good small areas of damage that have been detected. Once this is done the surface will be prepared for fitting the new material of the patch.
Nigel
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...