The weather has warmed and so has the interest on the RI 2612. Last week, Brian Paterson and Brian La Kemper preformed a single car air test on the coach and found a pair of leaks that must be repaired before the coach can be placed back in service. This weekend found the both of them repairing those leaks. This involved replacing a leaking angle cock and an air line "T" fitting. In this case, like most of the older equipment, the replacement of the pipe became more involved. Helping the two Brian's was young Phil from the steam shop. Together they had to remove twenty feet of air line pipe in order to repair the damaged "T" fitting. Nothing is easy! Hopefully, with the help of Tom Schneider and other steam shop members a new pipe will be bent and installed next weekend. My thanks for all those helping to make this repair!
And on the exterior...... Last Wednesday, Austin Harvey, began needle chipping the second vestibule. Saturday, Howard and Mary Gierer continued the chipping and removed almost 2/3 of the old yellow paint from below the belt rail. Thanks to all three of you for your continued efforts. We hope to continue prepping this side for the eventual painting of the Pullman green color this year. Would you like to join us? It seems as if Wednesdays are the perfect time for midweek activities at Irm. If you can't make on a Wednesday I am also at the barn 3 most Tuesday's and Thursday's. As always, I enjoy helping you, the volunteer, get started on a project. Please stop by Barn 3 for a visit and view our progress! Roger
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...