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Wednesday, May 14. 2014
Steam Department Update 05-12-2014 Posted by Nigel Bennett
in Steam Department at
07:18
Comments (21) Steam Department Update 05-12-2014A brief update this week as I was away in Cleveland at the weekend. The update is based upon input from Phil and Jim. Unfortunately the key conclusion from the week is that we will not be able to run next weekend, which was the first that we had scheduled for operation this year. We are pretty much “day to day”. #1630 is complete and ready to steam aside from refitting the smoke box front and the bell / lamp fittings mounted on it. The key activities have been repairing the cracks recently detected in the smoke box front casting. This is approaching completion but has been a much slower job than anticipated as the casting proves to be iron rather than steel. It must therefore be brazed rather than welded (a much slower process). Aside from other issues, brazing requires working from both sides so the huge casting had to be turned over part way thru the process. While Dennis was working on this:
So, work continues during the week and we will be in service as soon as the smokebox door can be refitted. Nigel Sunday, May 4. 2014
Steam Department Update 05-03-2014 Posted by Nigel Bennett
in Steam Department at
20:22
Comments (10) Steam Department Update 05-03-2014
As expected, the completion of the spraying last weekend opened up a frenzy of activity. Work got under way Tuesday and Wednesday once the paint was thoroughly dry. Almost all activity was on 1630 and she now looks a very different locomotive from last weekend. Even so, much of the critical progress is not visible.
On Tuesday and Wednesday work focused on preparing the boiler for hydro testing. This involved fitting the various water connections, valves and gauges to allow the boiler to be completely filled with water and then pressurized.
In addition the large copper pipe, that connects from the top of the firebox to the water column in the cab, had to be refitted. Once all this was done, the boiler was filled and water circulated thru the pool heater to bring the boiler up to around 100F for the pressure testing.
While this was being done Jerry and his son made huge progress in fitting the banding that secures the edges of the sheet metal on the barrel and firebox.
On Wednesday a pressure test was carried out. People have asked why this was necessary as #1630 was hydro and steam tested last year. What is happening now is not a full hydro test of the boiler shell (which requires testing at operating plus 25%) but rather checking for any leaks that may have developed as connections have been separated and remade over the Winter. For this we test only at operating pressure. The test served its purpose!. On Wednesday we found leakage around the connections of the pipe to the water column at both the first test and an attempt to re-seal it.
However, while this was going on, Phil and I made progress in refitting the injector starter valves.
Clearly on Saturday the first priority was to fix the connections of the offending pipe. Eric, Brian and others spent a lot of time thoroughly cleaning the seats and pipe ends of the connections, annealing new copper washers and then carefully re-fitting the pipe. It is a bear to fit as it is long, bent to fit around other equipment and fitted between two rigid seats. So, if it not exactly aligned, the seals at one or both ends do not seat correctly and leak.
Anyway, all the effort paid off and, during the afternoon, she was successfully pressure tested at 180 psi. This allows us to go ahead with the final steps to remove the hydro connections and install the remaining parts needed for operation (safety valves, brick arch etc.).
A lot of other work progressed in parallel with the pressure testing:
The biggest and nastiest job was refitting the two big air tanks under the walkways. These tanks weigh about 300 lbs and are each suspended by three “U” shaped steel rings the open ends of which pass thru the walkways to be secured by nuts.
The fitting is a “masterpiece” of the pipefitter’s art. The tanks must be squeezed into a confined space above the valve gear. The tanks are wider than the walkways so the supports are not simple “U”’s that could be passed around the tank .
Then change in a few days since the picture further up in this note is substantial.
The shape of each support is unique to its location and mixing then up can lead to the need to pull back the tank and start over again!. By evening they were both in place although the frustration during the day had reached considerable heights!.
The job of spotting and making good areas missed in painting continued. A lot more of this will hopefully happen next weekend when we expect to move the locomotive at least a little and reveal areas of the wheels that have so far been hidden.
The fireman’s gauge glass, that has been thoroughly cleaned and rebuilt, was refitted and showed no leakage under pressure.
The injector starter valves and their large connecting pipes were largely re-installed.
Front sander discharge pipes were re-installed.
Work progressed steadily on the smoke box. This is probably the area that most threatens our target to run on May 17th. Dennis, assisted by Christian and Jason completed the adjustment of the new steel sheet sections around the blast pipe. By end of day the sheet sections were being finally installed on to the mountings that had been welded into the smoke box and work was progressing on the mesh sections and the welded mounts that will attach these to the smoke box and complete the spark arrestor assembly.
The unexpected task that may cause a delay is in the smoke box front casting itself. Close inspection of this has indicated hairline cracks between the studs that secure the bell mounting. These will need to be weld filled, ground down and then the holes for the studs re-drilled and tapped before we can remount the front of the smoke box. It will be a busy two weeks.
So, we are close. A couple of key tasks will determine if we can steam in two weeks as planned.
I am away next weekend so will follow the action with great interest!.
Nigel
Sunday, April 27. 2014
Steam Department Update 04-26-2014 Posted by Nigel Bennett
in Steam Department at
18:45
Comments (10) Steam Department Update 04-26-2014
It was a very successful weekend in the steam shop. Although strictly not many of us were “in the steam shop” for very long on Saturday!.
Dennis and his son Keith, assisted by Jerry, Rick and others as required, occupied the shop to do the long awaited spray painting of #1630. The rest of us kept well away while this was going on.
The results are impressive. It took a little while to set up and test the new sprayer and the epoxy medium.
However, once this was done, progress was remarkable rapid.
By mid-afternoon everything was done. All the loose parts, tanks, dome cover and the banding strips were done. We are spraying only the back of the tender.
She really looks good. A great job by Dennis and Keith.
Unfortunately it is very clear that a plain shiny black locomotive does not photograph nearly as well in an enclosed shop as does one with all sorts of different colored patches!.
On Sunday, Jim and a small team removed all the masking so she is now looking much more like a finished locomotive.
Now we wait to confirm how long it will take for the epoxy medium to get thoroughly hard so that we can fit the plugs and valves into the top of the boiler to do the hydro test.
The rest of the team concentrated on getting a supply of water and proving the pool heater ready for the hydro test. The water car was switched to the front of barn #9 and filled using a very long run of pipe. (It cannot be located to the steam lead as the switch is being repaired and that area of track is out of service). However, this worked well and by afternoon the water car was full and back in front of the shop ready for use.
A temporary arrangement was set up to run water from the car thru the heater and back to the car to test the heater. Clearly Jerry did a great job last year!. The heater has traditionally been a bear to start up after the Winter. This time we simply started the water flow, switched it on and 30 seconds later it fired up and ran smoothly.
So we are all ready to put water into the boiler and heat it up for the testing as soon as we are confident that the paint is hard enough to allow us to access the boiler and make the connections.
We can now begin a whole lot of activities needed to refit all the small items removed to allow painting and make her ready for operation. It will be a busy couple of weeks!. Nigel
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Comments
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
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7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
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