Monday, March 15. 2010
Track Dept Weekend Report. March 14, 15 Posted by Adam Robillard
in Track Department at
15:24
Comments (0) Track Dept Weekend Report. March 14, 15Saturday Report from Adam Robillard and Sunday Report from Frank Devries: --------------- Today was just one of those days things just seemed to go right. It's about time I'd say. The day started early with Frank and myself and the first order of business was to make a run to Farm & Fleet for some hydraulic oil and parts. While we were away, JD Marzec and Greg Frech both showed up willing to work! They did some invaluable work 'derusting' and lubing track bolts in the shop and did a fine job. Upon our return we hit the machine maint. work. Frank filled the hydraulic on the switch tamper and began testing the new pump he had installed previously. Unfortunately it turns out the pump is pumping the wrong direction... a bit more trouble shooting and adjusting will be needed to hopefully get the machine back to 100% soon. JD, Greg and I topped off the hydraulic on the 6000 tamper and about that time Tom Hunter joined the gang. We did some QC bolt work on the 6000 and cleaned up the tool boxes and prepared to tamp.. The original plan was to do a walking inspection of the main line but the hit or miss weather was enough to keep us close to home.During lunch we formulated a plan for the rest of the day. Frank, JD and Greg set to do an oil/ filter change on the Amtrak Ballast regulator which desperately needed it. The air filter is the color of dirt and as Frank put it "hasn't seen daylight since the Carter Administration..." Tom and I ran to Napa for oil and filters and Frank, JD and Greg prepped the machines in Yard 11. While that gang was doing the oil, Tom and I switched out the 6000 tamper and began tamping the Streetcar line between Electric Park and the S-Curves. The initial goal was to test the machine from its winter work and break it back in. Amazingly everything seemed to work well and only a few minor adjustments will have to be made. We spent the next four hours tamping the carline and after the Regulator was finished Frank, JD and Greg ran it around to our work area and began regulating the freshly tamped track. Jeron Glander joined the gang later in the day and did a great job running the regulator after JD and Greg needed to leave. The four of us worked well into the evening hours surfacing the track with our recreation of an Amtrak surfacing gang. The ballast regulator made it through the day but the backlog of work continues to pile up. A few things fell off the machine unexpectedly but nothing to stop the machine from working. By the end of the evening we had the track fully tamped and a majority of the regulating complete. Some more work will have to happen in the daylight but otherwise it is mostly complete. Its amazing how much work can be done with a few good machines and a great crew. Next up we'll begin tamping the mainline... There is plenty of surfacing work there to keep us busy for a while. Thanks to all who helped today. We accomplished an incredible amount of work, far more than any of us expected. Thanks, Adam Robillard -------------------------------- More of the same...... The first task was to determine the electrical short on the regulator. When the lights were knocked off during the barn 11 project, the one light was hanging by the wire. Seems during our work on Saturday, it came in contact with the muffler, burned through the insulation and shorted. Jeron had noticed the high amp readings Saturday night. A quick clip of the wire resolved the short. The light bulb was broken in that light anyway. I noticed most of the lights are burned out on the machine. Next trip out I will pick up some spares from Napa. We fired up the regulator and resumed the plowing and brooming of the carline between Electric park and the S curve. After a short period of time Jeron noticed a hydraulic leak. I sent him back to yard 11 to put the machine away. Jeron found the leak was a loose hydraulic hose, and with quite a bit of trouble, tightened up the loose connection. Apparently like all track machines it was not as easy as putting a wrench on and tightening. From what I understand it involved a hydraulic power pack unit, and a lot of contortionist like moves. Once fixed, it was back to work. Brooming and plowing continued until another leak was noticed. Seems the valve for the oil pan had worked itself loose. When the leak was noticed we shut down quick, and resolved the leak. So that machine had it's second oil change this weekend. I will hit up the hardware store to get a plug for that valve to avoid a similar issue from happening again!!! By the end of the day the track looks really good. There is still a bit of box work to be done, but it is a huge improvement. While Jeron was fixing the hydraulic leak, I went for a walk. Track walking that is... I was able to inspect from East Station switch to Signal 251. During that walk, I found several loose joints, a couple of hanging joints that will get fixed when we tamp, but no breaks, no other defects that will affect opening day. I also marked several piles of OTM and scrap along the main for pick up with the 50. Brush through this stretch looks good. A touch up could be in order around Karsten's, but that's about it. I also marked ties for replacement between E. Station and Karsten's. I think the total was around 140 ties. I marked 5 ties off the bridge to ensure we have good support going into the bridge. Photos have been posted of the Carline results in the gallery below. A few shots of things from barn 10 as well. http://www.irm. Frank D. Monday, March 15. 2010Library Update - March 14, 2010One of our important elements in providing services to our members and in fulfilling our educational mission is the operation of the Strahorn Memorial Library, off campus, in nearby Marengo, IL. There you will find a dedicated group of volunteers and an AMAZING collection of railroad related items. Here is a short photo tour courtesy of images from Gwyn Stupar. Here is the main entrance. The building was constructed as the local public library and later the Museum was able to purchase the building. Some of the magazines reside on shelves that we salvaged from the Mount Prospect High School library. They have been refinished, restored, and assembled to provide additional space for the collection. The Strahorn has a comprehensive collection of Official Guides, as well as many Official Railway Equipment Registers. You will find some rare examples of paintings and railway art, some museum quality models, thousands of archived photos and negatives, and well over 15,000 railway and technical books. This is not a lending library, but has regular hours two days per week for walk-in visitors and other times by appointment. It is wise to call ahead as they depend on volunteer staffing, and at least during the winter, really bad weather can cause the open hours to be changed. If you have not been to this IRM operation, you owe it to yourself to visit, help out, or both of the above. Monday, March 15. 2010 |
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Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]