Sunday, April 6. 2014
Steam Department Update 04-05-2014 Posted by Nigel Bennett
in Steam Department at
17:53
Comments (12) Steam Department Update 04-05-2014
Back to Union after a couple of weeks in the UK. Lots of progress in the last two weeks and a hectic day on Saturday. The site looks very different with the snow gone and a frenzy of activity leading up to opening day. It is not normally this bad but the weather delays mean that work normally done in February and March has been concentrated into just a few weeks.
Frank and the track team, with assistance from the scouts camping on site, were hard at work on the track of the steam lead. This has proved to be a nightmare. The section of track in front of the service box car was very poor and was lifted in December to set new ties. Unfortunately the area was then covered by snow and has only just re-appeared!. On Saturday the new track was laid and we now have excellent track in the area where we will service 1630. This overcomes concern that, after all the work in the last couple of years, she could have fallen thru the track in her service area. Many thanks to Frank and his team.
(Thanks to David for the above pictures)
Unfortunately this is not the end of the job. We have only recently become aware that the big T&NO 2-10-2 (#975) rode up on the switch between the steam lead and the car line when being moved for the Transformers filming. Substantial work is required to repair this switch over the next few weeks and we will work with Frank’s team on this. However, we may need water for testing before this is done and the water car was stuck in the yard behind the damaged switch. So a very careful piece of switching was done under Frank’s supervision to pull the water cars out over the partially repaired switch with the BrownHoist. All went smoothly and we now have the water cars by the shop and can get water when required.
Another interesting exercise followed!. The damage highlighted the next major question. Why did #975 cause such damage when moved?. She was moved at short notice and without steam department staff present so we did not see the event. After an hour with a lot of oil and much shunting of #975 back and forth on the “Y” with the BrownHoist we think the problem is identified and resolved. Absent lubrication, the bearing plates of the trailing truck were not moving. After applying a lot of oil and pushing slowly in and out of the curve, there was an loud bang and the truck started moving from side to side again. More oil and a few more trips back and forth into the curve and she slides smoothly from side to side. A big 2-10-2 will never be happy on the curves around our site … but if lack of lubrication before movement turns it into a 2-12-0 !!!.
(Oh well. I have just heard from Jamie that we investigated the wrong locomotive. It was #2707 not #975 that damaged the switch. At least #975 is now well lubricated!.) Back in the shop the main effort was focused on preparing 1630 for spraying of the cab and boiler. A lot of different tasks were progressing in parallel.
Jim and Rick were filling and sanding areas of the cab side. In the past two weeks, Dennis has done a lot of weld repairs to the cab sides and these are now being finally prepared for spraying. While I was away, the decision was taken to remove and repaint the lettering, as it was proving too difficult to preserve the existing letters. So the cab sides are now completely stripped and stencils are being prepared.
Eric and many others worked on sanding down and masking the superstructure of the locomotive. The smokebox is now sheeted to protect it from over spray. All brass pipes and fittings, that are not to be sprayed, have been either removed or protected.
The injector starter valves were removed from the sides of the firebox, as these were too large and tricky to spray around.
The cab front windows are masked. Now we are ready for the painter to review readiness to actually do the spraying.
Jason, Collin and others worked on the smokebox front. Some leaks were detected in this during the November test runs. We had considered removing the front sheet and fitting a thicker gasket. However, the team identified that the leaks were clearly identifiable to a small number of specific areas, visible when Collin was shut in the darkness of the smoke box and lights were held on the outside!. These were sealed with a high temperature sealant. So this issue should now be resolved without the need to lift off the smokebox front again.
One of the large areas that has been completed while I was away is the top of the tender. This is not an area usually seen by the public, but it sure looks good despite a couple of Nigel’s dusty boot prints!.
Aside from 1630 most of the effort was focused on the switching to bring the water cars to the shop and resolve the issue with #975. However, in the shop:
Tom was working on the adjustments to the planer. It has actually been set up to start some work (the axle box for a leading truck). However it is not currently advancing the cutter horizontally or vertically between cutting strokes as it should. So work is progressing to work out why this is and how to correct it.
I worked with Collin and Bob on the new house air compressor. We now have most of the parts in hand for this and will plan to activated it soon.
While the trip to the UK was largely for a family visit, I was able to fit in a couple of visits to UK railways.
At the Bluebell Railway in Sussex I was warmly welcomed by a couple of the teams building largely new steam engines. The 84030 team are building a replica of an extinct class of BR 2-6-2T locomotive from parts of a similar 2-6-0 while the Atlantic team are building a replica of a 1911 LBSCR 4-4-2 using a boiler that survived in industrial use. In the latter project much of the rolling chassis is now complete. The new axle boxes and wheel make an interesting comparison to our efforts with #428.
The cylinders have been fabricated and are in place on the frames.
High quality work is obvious on the Bluebell in the wood working as well as the locomotives. These are shots of a superb set of late 19th century Metropolitan Railway varnished wood coaches, the restoration of which has won awards. These have been rebuilt in recent years from an extremely run down condition.
I subsequently visited the Severn Valley Railway for the last day of their Spring gala with 7 or 8 locos in steam. A pause to wait the crossing with another train gave me the chance to look closely at one of their GWR Manor class locomotives. It really highlights how different the layout and painting of this is when compared to our #1630. Looking in this way, there is no exposed pipework. It all runs below the sheet metal, which is almost completely unbroken. A very different approach when I think of all the holes that we have to adjust and fill around the many pipes and studs on our locomotive.
There was no work at the shop on Sunday as many of us attended the memorial for our late and sorely missed friend Bill Chyna. Many thanks to Kath and Beth for the invitation to a very pleasant afternoon remembering the good times.
Next weekend is likely to be rather quiet as many people will need to attend the rules training and / or test in preparation for running this season.
Nigel
Sunday, April 6. 2014
March 30th, Warm Weather Strikes IRM Posted by Pauline Trabert
in Passenger Car Department at
11:43
Comment (1) March 30th, Warm Weather Strikes IRMOn Friday, March 28th, Shelly Vanderschaegen worked with Wayne Baksic at his home to apply hardware to a seat back for a Rock Island coach which Shelly has reupholstered in her home workshop. On Sunday, March 30th, Shelly and Kevin Kriebs began the day by cleaning the Pacific Peak and got half way through the car by the end of the day. Ray Mormann and Coach Department Curator Michael Baksic were tracing elelctrical wiring in the Birmingham kitchen to understand which switches work with which lights and outlets. Mark Gellman and Michael McCraren worked on the overhead panel in the vestibule of the RDC and then they put tools away from the Pacific Peak so that Shelly and Kevin could clean in there. Michael M. left after lunch.
Bob Hunter stopped by to chat with Michael Baksic and joined the crew for lunch in the Birmingham diner and discussed carpeting for the Dover Strait. Jon Habegger brougnt in pictures that will go in the Birmingham and worked out where to put them. Jim Windmeier provided assistance to Jon in the Exhibit Car. The Chicago depot article from NRHS was rehung. Jim and Jon talked at length about potential displays that can be created during 2014 and installed before the 2015 season. Mark Hoffman spent Sunday priming the ceiling in the John McLoughlin where he had previously done needle chipping. In the Ely, Buzz Morisette has put all three ceiling panels up and applied joint compound. Once sanded and smoothed, then primier will be applied and then everything will be painted. Shelly Vanderschaegen captured an image of nearly the entire ceiling while laying on the floor. |
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Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
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Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
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Sat, 04-17-2021 23:07
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Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
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Fri, 04-09-2021 19:56
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Wed, 03-31-2021 11:37
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