While the 504 and 1848 were still in the heated shop to keep them from freezing, Jeron and I decided to work on a few little things that have needed attention. On the 19th, Jeron removed, cleaned, and reassembled the automatic air drains on the main reservoirs, and along the way found out that one of them to have a small crack in the housing near the manual part of the valve. It will be replaced later this winter. He also tracked some some other small air leaks, repairing some and noting some others for future repairs. There was a copper pipe on the drain side of an auto drain that had a split to it, that was soldered shut and put it back in place.
Meanwhile, I started working on the air brakes. An issue started to occur where the independent brake would not stay bailed off. The fix here was to replace the 26-F quick release valve and the control valve which had a slight leak to it. At the same time a couple of filters on the air system were replaced. There is one more issue where we are waiting for a valve to ship from PABCO.
Last night we spent a couple hours at the shop doing a little more TLC work on 504 and 1848. On 504, the platform crosswalk lights never had the lenses put in from when the restoration was completed years ago. They were just blanked over for the painting. I used one of the old fogged lexan windows from the bilevels and cut out a couple squares with the sawzall for the front and rear. Screwed and sealed it with some clear silicone so water won't get into it, let it dry and screwed the plates, with lenses, back in right before leaving for the night. The radio had quit working earlier this year, but we never had the time to troubleshoot why. A little bit of looking this time found no voltage at the radio rack and nothing at the radio breaker. Traced the wires back further into the cabinet only to find a broken one near the knife switch. Placed a butt splice on that and the radio works again. Jeron replaced a bulb on the transmit indicator as well.
On the 1848, Jeron rebuilt one of the rear sander magnet valves that was sticking and leaking a bit. There is still more to do on these after some rebuild kits are ordered. We also straitened out one of the rear break away stanchions for the crosswalk safety chains that was not exactly straight.
Over the next couple weeks, some other items will be done on both units before they get moved out of the shop and other equipment comes in for work.
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...