A great deal of work was done in the steam shop during the week and over the weekend. Unfortunately, on Saturday, we hit a snag that may hold us up significantly.
The information this week is provided by Phil and Brian as I am far away on vacation. Thanks guys.
On 1630, Brian Davies is now working full time and, with JD, Jerry, Cameron, Jeff, Jason and others all spending time working with him during the week the locomotive has seen a lot of changes:
· The air system was all back together with the exception of the compressor by Friday. After a few fits, the brakes work!
· Mike was working to finish that on Saturday ready for testing. Later in the day the house air was hooked up and the air pump was tested. At first the high pressure steam side moved once and then it froze up. The stuffing boxes were loosened and oil was put on the pistons. A second attempt was made. It worked beautifully. So, it was good to see that something be confirmed as done and working on the locomotive.
· All of the sheet metal in the cab is on. Some screws still need to be added. With the exception of attaching and plumbing the stoker jet manifold, the cab is basically complete!! Even the electric is hooked back up pending testing.
· Cylinder cocks have been cleaned and inspected, and a new pipe nipple installed after one broke. They should be good to go.
· Jim and Brian are added the last little bits of insulation around about the last foot of flexible stays on either side of the wrapper sheet.
· Sheet metal, minus the bands, was completed across the barrel.
· On Saturday much of the banding was fitted.
· The final normal hydro was performed yesterday to hammer stay bolts. This proved good so no issues with these.
· The blow down muffler was installed.
· Preparations have been made for the steam test including:
o Setting up a large steam valve on the pipe coming off of the auxiliary dome lid to allow a gauge to be fitted for testing the safety valves; and
o Making two gags that will allow individual valves to be held closed to allow the others to be tested.
· Unfortunately the key objective on Saturday, which was to apply hydro pressure to the front end to test the sealing of the super heater elements into the header, ran in to significant problems. This relies upon pressurizing the whole front end (cylinders, valve chambers, exhaust passages etc. with water to about 50 psi). This involves minimizing water leakage thru a whole lot of areas, such as the piston glands, that are not wholly tight under steam and are a lot more problematic using water.
· A large team spent the morning preparing for the test and the first filling was carried out in the afternoon. This indicated a lot of leakage around the piston and valve glands as well as the junction where the exhaust steam from the air compressor and stoker enter the cylinder casting.
· Water was them lowered so fixes could be made to seal the water better. While some progress was made on the glands it was found that the exhaust steam connection, which is in a really awkward place under the boiler, could not be sealed in a way that allowed a pressure of anything like 50 psi to be achieved. This is a complex threaded assembly on which the threads proved to be damaged.
· To progress the test it will now be necessary to machine a replacement part. At the same time further work will be done on the packing glands of the piston and valve rods. After this we can again try to pressurize the front end and test the sealing of the super heater elements.
On 428:
· Tom has finished most of the machining on the wedges. All that is left to do is to drill several hole in them so that they can be adjusted when they are put on the locomotive. Brian and Cameron made a mount that will align for the drilling of these holes.
· The mounting brackets for 428's air compressor received a coat of paint.
In other areas:
· Stu, Bob, and Jane worked on painting the planer. It looks quite remarkable now that it has green paint on it. Bob also worked on assembly of some more small pipes.
So a lot was accomplished during this week. If we can successfully test pressure test the front end, we are just about ready to steam test.
Sitting here in Australia!!, I will wait with bated breath for updates on progress with the front end testing.
Nigel
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...