A great deal of work was done in the steam shop during the week and over the weekend. Unfortunately, on Saturday, we hit a snag that may hold us up significantly.
The information this week is provided by Phil and Brian as I am far away on vacation. Thanks guys.
On 1630, Brian Davies is now working full time and, with JD, Jerry, Cameron, Jeff, Jason and others all spending time working with him during the week the locomotive has seen a lot of changes:
· The air system was all back together with the exception of the compressor by Friday. After a few fits, the brakes work!
· Mike was working to finish that on Saturday ready for testing. Later in the day the house air was hooked up and the air pump was tested. At first the high pressure steam side moved once and then it froze up. The stuffing boxes were loosened and oil was put on the pistons. A second attempt was made. It worked beautifully. So, it was good to see that something be confirmed as done and working on the locomotive.
· All of the sheet metal in the cab is on. Some screws still need to be added. With the exception of attaching and plumbing the stoker jet manifold, the cab is basically complete!! Even the electric is hooked back up pending testing.
· Cylinder cocks have been cleaned and inspected, and a new pipe nipple installed after one broke. They should be good to go.
· Jim and Brian are added the last little bits of insulation around about the last foot of flexible stays on either side of the wrapper sheet.
· Sheet metal, minus the bands, was completed across the barrel.
· On Saturday much of the banding was fitted.
· The final normal hydro was performed yesterday to hammer stay bolts. This proved good so no issues with these.
· The blow down muffler was installed.
· Preparations have been made for the steam test including:
o Setting up a large steam valve on the pipe coming off of the auxiliary dome lid to allow a gauge to be fitted for testing the safety valves; and
o Making two gags that will allow individual valves to be held closed to allow the others to be tested.
· Unfortunately the key objective on Saturday, which was to apply hydro pressure to the front end to test the sealing of the super heater elements into the header, ran in to significant problems. This relies upon pressurizing the whole front end (cylinders, valve chambers, exhaust passages etc. with water to about 50 psi). This involves minimizing water leakage thru a whole lot of areas, such as the piston glands, that are not wholly tight under steam and are a lot more problematic using water.
· A large team spent the morning preparing for the test and the first filling was carried out in the afternoon. This indicated a lot of leakage around the piston and valve glands as well as the junction where the exhaust steam from the air compressor and stoker enter the cylinder casting.
· Water was them lowered so fixes could be made to seal the water better. While some progress was made on the glands it was found that the exhaust steam connection, which is in a really awkward place under the boiler, could not be sealed in a way that allowed a pressure of anything like 50 psi to be achieved. This is a complex threaded assembly on which the threads proved to be damaged.
· To progress the test it will now be necessary to machine a replacement part. At the same time further work will be done on the packing glands of the piston and valve rods. After this we can again try to pressurize the front end and test the sealing of the super heater elements.
On 428:
· Tom has finished most of the machining on the wedges. All that is left to do is to drill several hole in them so that they can be adjusted when they are put on the locomotive. Brian and Cameron made a mount that will align for the drilling of these holes.
· The mounting brackets for 428's air compressor received a coat of paint.
In other areas:
· Stu, Bob, and Jane worked on painting the planer. It looks quite remarkable now that it has green paint on it. Bob also worked on assembly of some more small pipes.
So a lot was accomplished during this week. If we can successfully test pressure test the front end, we are just about ready to steam test.
Sitting here in Australia!!, I will wait with bated breath for updates on progress with the front end testing.
Nigel
Comments
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]